The Smell of Molten Projects in the Morning

Ed Nisley's Blog: Shop notes, electronics, firmware, machinery, 3D printing, laser cuttery, and curiosities. Contents: 100% human thinking, 0% AI slop.

Tag: Mini-lathe

Tweaking an LMS 5200 Mini-Lathe

  • Screw Cutting Fixture vs. Lathe Ways

    A length of aluminum hex bar became a nice 10-32 screw trimmer:

    Screw cutting fixture - 10-32 - first cut
    Screw cutting fixture – 10-32 – first cut

    The hex neatly fits a 5/8 inch wrench, so I can tighten the jam nuts enough to run the lathe forward, part off the screw, and clean up the end just fine.

    Unfortunately, the second test cut didn’t work nearly so well:

    Screw cutting fixture - 10-32 - wrecked
    Screw cutting fixture – 10-32 – wrecked

    With the cross-slide gib adjusted to the snug side of easy, the cut put enough pressure on the parting tool to lift the way on the tailstock side about 4 mil = 0.1 mm. The parting tool submarined under the cut, dislodged the fixture, and didn’t quite stall the motor while the chuck jaws ate into the aluminum.

    Well, that was a learning experience.

    After tightening the cross-slide gib to the far side of hard-to-turn:

    • Put a longer screw in the fixture
    • Grab it in the tailstock drill chuck
    • Crunch the hex end of the fixture in the spindle chuck
    • Remove the screw through the spindle (*)
    • Put a slight taper on the end of the fixture threads with a center drill
    • Deploy the live center to support the fixture

    Like this:

    Screw cutting fixture - 10-32 - rechucked
    Screw cutting fixture – 10-32 – rechucked

    Turns out that angling the bit by 10° dramatically reduces chatter. If I had BR and BL turning tools, I’d be using them with the QCTP set to 0°, but they weren’t included in the set that came with the lathe.

    It’s a good thing I’m not fussy about the diameter of that cylindrical section:

    Screw cutting fixture - 10-32 - reshaped
    Screw cutting fixture – 10-32 – reshaped

    I knew the craptastic lathe ways needed, mmmm, improvement and it’s about time to do something.

    (*) By concatenating all my ¼ inch socket extension bars into an absurd noodle capped with square-to-hex adapter holding a Philips bit.

  • Screw Cutting Fixture: Full-thread Aluminum

    By and large, when you follow the recipe, you get the expected result:

    Screw cutting fixture - M3x0.5 aluminum - side view
    Screw cutting fixture – M3x0.5 aluminum – side view

    That’s another length of the same aluminum rod, this time with a full-length M3x0.5 thread down the middle, and a screw with a neatly trimmed end.

    Running the lathe spindle in reverse prevents the screw from loosening the jam nuts on the left:

    Screw cutting fixture - M3x0.5 aluminum - in lathe chuck
    Screw cutting fixture – M3x0.5 aluminum – in lathe chuck

    Running the spindle forward does move the screw enough to loosen the nuts. Perhaps I should put wrench flats on the big end of the fixture so I can really torque the nuts.

    That front nut was mostly decorative, rather than tight, because I didn’t expect the first attempt to work nearly as well as it did. A bit of filing to taper the end of the thread and it was all good.

    That was easy…

     

  • Kenmore 158: Presser Foot Tweak

    After watching Mary fiddle with the shrunken presser foot screw, I tapered the tip as a guide into the hole:

    Presser Foot Screw - tapered tip
    Presser Foot Screw – tapered tip

    A hint-and-tip (which I cannot, alas, find again) suggested making bushings to simplify trimming screws in the lathe. A rim on the bushing aligns it with the front of the jaws, the screw threads into the central hole with a jam nut locking it in place, then you can turn / shape / file the end of the screw just beyond bushing with great support and a total lack of drama.

    For the moment, I just aligned the screw in the tailstock drill chuck, crunched the three-jaw spindle chuck on the screw head, backed off the tailstock, took unsupported sissy cuts, and it was all good:

    Presser Foot Screw - chuck alignment
    Presser Foot Screw – chuck alignment

    Gotta make those bushings!

  • Respooling Stainless Steel Thread: The Knack

    The comments on my previous stainless-steel thread respooling attempt suggested that I was entirely too much of a sissy, so, when another empty spool appeared, I tried again with more vigor:

    Stainless steel thread - second spool
    Stainless steel thread – second spool

    As before, I put the larger spool on the floor under the lathe and let the thread spill straight off the top toward the smaller spool. This time, I didn’t have a twist accumulating in the loose thread between the two spools:

    • Grab longer lengths of the loose thread
    • Absolutely no slippage between the fingers!
    • Put more tension on the thread at the takeup spool

    As nearly as I can tell, the thread still has a slight twist coming off the larger spool, but grabbing longer lengths captures the twist and more tension lays it on the smaller spool. After cutting the thread, what was left had maybe three turns of twist, which was no big deal and obviously hadn’t accumulated.

    Seems better: thanks for all the comments!

  • Fordham FG-801 Function Generator Power Switch

    The power switch in my trusty Fordham FG-801 Function Generator failed with an accumulation of oxidation / crud on the contacts. That’s fix-able, but the switch contained not one, but two powerful springs, and puked its guts all over the floor around the Squidwrench Operating Table. Even with (a preponderance of) the parts in hand, I couldn’t figure out how to reassemble the thing; the only way out was to replace the switch.

    The OEM switch had a 0.360+ inch diameter pushbutton that fit into a ⅜ inch hole and, alas, my remaining stock of line-voltage switches had toggle levers and used ¼ inch holes. So I converted a bit of aluminum rod into a suitable bushing:

    Fordham FG-801 Fn Gen - new switch hardware
    Fordham FG-801 Fn Gen – new switch hardware

    The lock washer in the middle started with a much wider tab that I filed down into a tooth for the dent from a #2 center drill. Protip: center drills don’t walk off like twist drills, even when you hand-hold the front panel at the drill press with all the electronics dangling below.

    The bushing dimension doodle:

    Fordham FG-801 Function Generator - Replacement Switch Bushing
    Fordham FG-801 Function Generator – Replacement Switch Bushing

    The internal wiring routes the 120 VAC line conductor to the switch, then to the fuse, then to the transformer. I don’t know whether it’s better to have an unfused switch or an unswitched fuse (surely there’s a UL spec for that), but I didn’t change anything. The new switch, being slightly smaller and mounting directly on the panel, required a new wire (the blue one) from the fuse:

    Fordham FG-801 Fn Gen - power switch - installed
    Fordham FG-801 Fn Gen – power switch – installed

    The OEM switch mounted on two round brass standoffs and, wonder to tell, the new switch fit between them!

    From the front, the new switch looks like it grew there:

    Fordham FG-801 Fn Gen - switch in action
    Fordham FG-801 Fn Gen – switch in action

    The PCB mounts to the top of the case with one screw and four hexagonal brass standoffs. The standoffs have 6-32 tapped holes on one end and a 6-32 stud on the other; one of those stud had broken off. A 6-32 stainless steel screw secured in a clearance hole with a dab of epoxy solved that problem:

    Fordham FG-801 Fn Gen - standoff stud
    Fordham FG-801 Fn Gen – standoff stud

    I stood it vertically and tweaked the screw to be perpendicular while the epoxy cured.

    Memo to Self: The next time around, put a nut on the stud to make sure the answer comes out right. I didn’t do this time to avoid epoxying the nut to the standoff.

    Done!

  • Respooling Stainless Steel Thread

    For various reasons, I needed a smaller quantity of that stainless steel thread / yarn, so I mooched an empty spool from Mary, ran a bolt through it with washers + nut on the far end, chucked the bolt in the lathe, and ran the spindle backwards at the slowest speed:

    Stainless steel thread - smaller spool
    Stainless steel thread – smaller spool

    I started by letting the big spool unroll from the side, but that produced horrible twists in the slack thread. Remembering the lesson from our previous thread spool adventure, I put it on the floor and let the thread pull from the top:

    Stainless steel thread - unwinding spool
    Stainless steel thread – unwinding spool

    It still accumulated a huge twist between the two spools, even while guiding it hand-over-hand onto the rotating spool. Either the factory lays the thread on the large spool with a built-in twist or, more likely, a multi-strand steel thread behaves like a spring, no matter what anybody wants, and comes off the spool with a nasty case of inherent vice.

    Memo to Self: don’t let stainless steel thread slide through your hands under power, because some of the fuzz visible in the top picture will stay with you.

  • Mini-Lathe: Electronics Box Screw Insert

    Two bags of knurled brass M4 inserts arrived from halfway around the planet, so I could fix the offending hole behind the LMS mini-lathe’s electronics box:

    LMS Mini-lathe - mistapped cover hole
    LMS Mini-lathe – mistapped cover hole

    Although you should remove the lathe from the chip pan and do it right, I gimmicked up a reducer for the long drill extension that, IIRC, came with the house:

    LMS mini-lathe - drill bit extension
    LMS mini-lathe – drill bit extension

    I figured that would be close enough, given the starting situation. The cast iron frame is perhaps half an inch thick at that point, with steel brackets bolted to the far side, so use the hole as a guide and don’t drill with wild abandon.

    A long M4 screw serves to align the insert eyeballometrically perpendicular to the surface while the JB Kwik epoxy cured:

    LMS mini-lathe - insert alignment
    LMS mini-lathe – insert alignment

    It definitely doesn’t look like it grew there and, indeed, looks like the obvious repair job it is:

    LMS mini-lathe - insert epoxied
    LMS mini-lathe – insert epoxied

    I thought about replacing all the screws, but decided it was so well hidden that, if I didn’t tell anybody, they’d never know:

    LMS mini-lathe - cover screw installed
    LMS mini-lathe – cover screw installed

    Done!