The Smell of Molten Projects in the Morning

Ed Nisley's Blog: Shop notes, electronics, firmware, machinery, 3D printing, laser cuttery, and curiosities. Contents: 100% human thinking, 0% AI slop.

Tag: Repairs

If it used to work, it can work again

  • Wall Switch Failure

    Here’s what happens to a really old wall switch:

    Wall Switch - innards
    Wall Switch – innards

    A closeup of that broken contact:

    Wall Switch - detail
    Wall Switch – detail

    This switch controlled an outlet, so I’m sure it’s hot-switched far too many vacuum cleaners, clothes irons, and suchlike over the last half century or so.

    Our house is a bit fancier and originally had top-of-the-line mercury-wetted switches: the contacts sealed in the capsule don’t burn, but the springy supporting structures outside the capsule eventually wear out.

    They’re still more reliable than X10 switches, though.

  • Furnace Heat Exchanger: Temporary Repair

    Which small spot on this hot-air furnace heat exchanger isn’t like all the other small spots?

    Pinhole in furnace heat exchanger
    Pinhole in furnace heat exchanger

    Correct! The orange one at the corner of the rectangular exhaust gas flue that’s lit up like the sun, because you’re looking directly into the oil burner flame.

    With the fire off and everything cooled down, it looked like this:

    Pinhole in furnace heat exchanger - detail
    Pinhole in furnace heat exchanger – detail

    Now, this calls for a new furnace (because replacing the heat exchanger costs as much as a new furnace), but as it turns out this was in an unoccupied house during the week before Christmas. So I scrubbed off the debris with a steel brush, bent up a snippet of 2 mil brass shimstock to fit the corner, applied a layer of JB Industro-Weld epoxy to the problem, and positioned 200 W of incandescent bulbs to help it cure slightly sooner than forever:

    Furnace heat exchanger - temporary fix
    Furnace heat exchanger – temporary fix

    That is most certainly not a final repair, not just because the heat exchanger’s normal operating temperature exceeds the epoxy’s 500 °F rating, but because where there’s one pinhole there’s bound to be more. The goal was to let us keep the furnace running until we could schedule the replacement after the holidays. Remember, the building isn’t occupied and neither of the smoke / CO detectors went off at any point in the proceedings.

    Houses are trouble!

  • HP3970 Scanjet Lid Hinge Repair

    When the second hinge on my father-in-law’s scanner broke, he asked if I could fix it:

    HP3970 Scanjet Lid - broken hinge
    HP3970 Scanjet Lid – broken hinge

    It’s a flatbed scanner, so the lid is nearly 18 inches long and weighs 2.2 pounds with the slide / negative backlight illuminator. The stress raiser notches, located exactly where the cracks started, look like a perfect example of how not to do these things.

    I solvent-glued the hinges back together, with a square brass tube applying clamping force to the joint overnight, but this certainly won’t last for long:

    HP3970 Scanjet Lid - crude repair
    HP3970 Scanjet Lid – crude repair

    HP used to have some really smart engineers, but this looks like it was done by a Newkid (I was one, once, so I know the type) after a solid modeling and simulation session convinced him that those two thin plastic webs had enough strength for the job.

    No. They. Do. Not.

    Of course, HP provides no Official Way to repair that failure, as the hinges emerge seamlessly from the injection-molded plastic lid frame: you must scrap the scanner and buy a new one, because the lid would cost more than a new scanner. Equally of course, the fact that they don’t have a Windows driver beyond XP makes replacement a foregone conclusion.

    It runs under Xubuntu 12.04, mostly, which is what I set him up with after the XP PC got compromised.

  • Commercial Line Cord: Details Matter

    Driven by forces beyond my control, I had to rent a carpet cleaner from a local Big Box home repair store. The rugged line cord plug had an unusual (to me, anyway) strain relief fitting on the back, consisting of a circumferential clamp around the cord and a large diameter, deeply recessed opening on the nut to prevent the cord from flexing sharply:

    AC Line Cord Plug - clamp nut
    AC Line Cord Plug – clamp nut

    But something seemed odd, so I unscrewed the finger-tight clamping nut:

    AC Line Cord Plug - clamp fingers
    AC Line Cord Plug – clamp fingers

    Whoever installed the cord cut the insulation back far too much, as those fingers should close on the insulation jacket, not the conductors.

    I fought down my instinctive response, took a deep breath, clicked my heels together three times, repeated “This is not my problem”, and suddenly it wasn’t my problem any more. I tried reporting it to the harried clerk at the Big Box Store, but she instantly fluttered off to help somebody else after noting my return in the Big Book of Rental Contracts.

  • HP10525T Logic Probe: New Timing Capacitors

    While putting together the PIR sensor, I had occasion to haul out the old HP10525T Logic Probe (a bookend for the Tek logic probe) to figure out why the shift register wasn’t updating; that was easier than hauling the breadboard to the oscilloscope. While it showed the problem (wire tucked into wrong hole, hidden behind a cluster of other wires), it didn’t seem to be blinking quite right. The HP10525T Logic Probe Operating and Service Manual says it should blink at about 10 Hz for any pulse train from about 10 Hz up through 50 MHz (yes, 50 megahertz), with a minimum pulse width of 10 ns (yes, 10 nanoseconds), but it didn’t do that for the PWM going to the RGB LED strip or the shift register clock.

    Given a manual printed in February 1975, I’m sure you know where this will end up…

    Unlike contemporary gear, the manual tells you how to dismantle the probe, using the needle tip as a tool. Doing so reveals a tidy circuit board with gold plated PCB traces:

    HP10525T - original caps
    HP10525T – original caps

    The two tiny black rectangular capacitors just to the left of the 8 pin DIP IC are C1 and C2, rated 10 μF at 2 V (yes, 2 volts). As you might expect, they had ESRs in the 3 to 5 Ω range, rather than around 0.2 Ω. The catch is that the case doesn’t have room for anything much taller, but I did contort some solid tantalum through-hole caps into the space available:

    HP10525T - replacement caps
    HP10525T – replacement caps

    Buttoned it up again and … it works fine. There really isn’t that much else to go wrong, is there?

    This picture shows the incandescent lamp glowing half-bright to indicate that the lethally sharp probe tip (on the left here, with its stud on the right in the other pictures) sees a floating input:

    HP10525T Logic Probe - glowing
    HP10525T Logic Probe – glowing

    I love happy endings, although I’m sure the accompanying HP10526T Logic Pulser needs recapping, too. When that project comes around, I’ll probably use SMD ceramic caps, because the pulser’s circuit board packs even more parts into the same volume.

    Speaking of unhappy endings, HP used to be run by real techies: The Fine Manual’s body starts with Page 0 verso, after the title and two pages of front matter. ‘Nuff said.

  • Ancient Harman-Kardon PC Speaker Re-Capping

    HK Powered Speakers - front view
    HK Powered Speakers – front view

    Suddenly a resonant thwup-thwup-thwup-thwup fills the house, but no helicopters fill the skies; in fact, most of the noise seems to be inside the house and … it’s coming from the shop. We look at each other and dash toward the basement door, knowing perfectly well that this is the part of the movie where the audience chants “Don’t open the door! Don’t open the door!

    Come to find out that it’s the pair of old Harman-Kardon powered speakers attached to the PC attached to the Thing-O-Matic; the PC is off, but I left the speakers turned on. Quick diagnostics: turning the volume down doesn’t reduce the motorboating, pulling the audio cable out of the PC doesn’t change anything, the only cure is to turn them off.

    Under normal circumstances, they’re pretty good-sounding speakers, at least to my deflicted ears, although I have my doubts about the effectiveness of that reflex port. I plugged in a pair of unpowered speakers as subwoofers down near the floor, just because they were lying around; a pair of 75 mm drivers does not a subwoofer make, fer shure.

    Pop quiz: what’s wrong?

    Need a hint? Looky here:

    HK Powered Speakers - wall wart
    HK Powered Speakers – wall wart

    Disassembly:

    • The front cloth grille has four snap mount posts, two secured by hot-melt glue blobs: pry harder than you think necessary
    • Two screws near the top of the bezel thus revealed hold it to the back
    • The bottom two screws holding the driver frame in place also hold the bezel to the back
    • Remove two screws from the grooves in the bottom of the back
    • Amazingly, the driver has two different size quick-disconnect tabs; the neatly polarized wires slide right off

    Cut the audio cable just behind the back panel, then push the two-piece cable clamp outward from the inside:

    HK Powered Speakers - cable grommet
    HK Powered Speakers – cable grommet

    The bottom of the circuit board shows considerable attention to detail. Note the excellent single-point ground at the negative terminal of the big filter capacitor:

    HK Powered Speakers - PCB foil side
    HK Powered Speakers – PCB foil side

    And, of course, that’s the problem: most of the electrolytic capacitors were dried out. My ESR tester reported the big filter cap (downstream of the bridge rectifiers) as Open and several of the smaller caps were around 10 Ω. Replacing them with similarly sized caps from the heap solved the problem.

    It should be good for another decade or two…

  • Samsung VAC-9048R Vacuum Cleaner: Floor Brush Rollers

    The hard-floor brush for our old Samsung VAC-9048R vacuum cleaner began scratching the hardwood floor, which called for some investigation & repair. The Fine Manual doesn’t even mention the hard floor brush, so it’s obvious I’m on my own (as is usually the case). Believe it or not, we actually discussed buying a vacuum cleaner, but the new ones have poor reviews, bulky & awkward plastic widgets on the handle, or suffer from other glaringly obvious faults; although this one is aging poorly, it’s at least workable. Plus, I bought a lifetime supply of bags when it was new and it’s not dead yet.

    So, we begin…

    The rollers that used to support the front of the brush have worn down, allowing the bottom cover to erode on the floor. The right side ran through something sticky in the recent past:

    Samsung 9048 - worn roller - right
    Samsung 9048 – worn roller – right

    The left side may not be sticky, but it’s in no better shape:

    Samsung 9048 - worn roller - left
    Samsung 9048 – worn roller – left

    Remove the two obvious screws, pry the front edge up, and the whole cover plate pops off to reveal the two rollers. They pull straight out of the shaft support brackets molded into the top frame. Even their metal shafts show grievous wear:

    Samsung 9048 - worn roller parts
    Samsung 9048 – worn roller parts

    The rollers consist of a hard plastic hub supporting a flexible rubbery tire, turning on a 3 mm steel shaft that’s worn on one side (which was downward, of course). The central holes in the rollers probably used to fit the shafts, but they’re now worn to 4 mm ID. The tires were probably a lot larger in diameter, too, back when they were new.

    A bit of rummaging in the Basement Laboratory Warehouse Wing produced a bag of vibration isolation bushings that had about the right consistency to become tires:

    Samsung 9048 - rollers and surplus vibration isolation bushings
    Samsung 9048 – rollers and surplus vibration isolation bushings

    They’re much larger than necessary, but are now, shall we say, fully depreciated and ready for a new, if somewhat downsized, lifestyle.

    Unfortunately, they don’t fit onto the existing hubs, so I can’t use the hubs as a template. Fortunately, I have a lathe and some random nylon stock (with crosswise notches that didn’t pose much of a problem):

    Samsun 9048 - turning roller hub
    Samsun 9048 – turning roller hub

    I came to my senses before converting this into a 3D printer project. If I had to make more than two hubs, it’d be a good idea to solid-model and print them, even if they’re just barely large enough to allow solid infill:

    Samsun 9048 - finished roller hub
    Samsun 9048 – finished roller hub

    I’d go for a 3 mm ID to increase the wall width; these have a 4 mm ID to fit the brass bushings described below. There’s no significant overhang and they’d print with no problems. Maybe next time?

    The isolation bushings cut easily with a sharp razor knife, so I pared them down to a bit over what I estimated to be the finished roller OD and width:

    Samsung 9048 - roller tire before grinding
    Samsung 9048 – roller tire before grinding

    The 10-32 screw in that shiny new hub serves as an arbor in the lathe, where I held a Dremel tool with a sanding drum down on the compound rest, ran the lathe at its slowest back-gear speed, and sanded the bushing down to what seemed to be the right OD for the tire:

    Samsung 9048 - grinding roller tire
    Samsung 9048 – grinding roller tire

    The white snout in front leads to a shopvac that caught most of the dust. The front of the lathe chuck shows it wasn’t perfectly effective and I should have worn a dust mask; my glasses didn’t collect much dust, so maybe my lungs didn’t, either.

    A trial fit in the floor brush body showed that this one was slightly too large and the sides needed tapering. The inside view:

    Samsung 9048 - ground roller before side trim
    Samsung 9048 – ground roller before side trim

    The outside view, with the cover just slightly unable to snap closed:

    Samsung 9048 - slightly oversize roller in place
    Samsung 9048 – slightly oversize roller in place

    Grinding a bit more off produced a pair of 15.5 mm OD tires which fit nicely. Some careful razor knife work smoothed and tapered the sides:

    Samsung 9048 - finished rollers
    Samsung 9048 – finished rollers

    Brass tubes (from the stash of cutoffs) compensate for the flat on the severely worn steel shafts; a fix that turned out to be much easier than building new shafts:

    Samsung 9048 - roller shaft bushing hub
    Samsung 9048 – roller shaft bushing hub

    Then reassemble in reverse order and it’s all good!

    I wrapped a layer of silicone tape around the large and slightly worn hard-plastic rear tires, even though I’m sure that won’t last very long at all:

    Samsung 9048 - repaired hard floor brush - bottom
    Samsung 9048 – repaired hard floor brush – bottom

    The shop doodle giving all the sizes:

    Samsung 9048 - Roller dimension doodles
    Samsung 9048 – Roller dimension doodles

    Now, if that doesn’t count as a gonzo repair, I don’t know what would… [grin]