The Smell of Molten Projects in the Morning

Ed Nisley's Blog: Shop notes, electronics, firmware, machinery, 3D printing, laser cuttery, and curiosities. Contents: 100% human thinking, 0% AI slop.

Tag: Improvements

Making the world a better place, one piece at a time

  • Baofeng UV-5R Squelch Settings

    The Baofeng UV-5R radios on our bikes seem absurdly sensitive to intermodulation interference, particularly on rides across the Walkway Over the Hudson, which has a glorious view of the repeaters and paging transmitters atop Illinois Mountain:

    Walkway Over The Hudson - Illinois Mountain Antennas
    Walkway Over The Hudson – Illinois Mountain Antennas

    A better view of the assortment on the right:

    Illinois Mountain - North Antennas
    Illinois Mountain – North Antennas

    And on the left:

    Illinois Mountain - South Antennas
    Illinois Mountain – South Antennas

    Not shown: the Sheriff’s Office transmitter behind us on the left and the Vassar Brothers Hospital / MidHudson pagers on either side at eye level. There’s plenty of RFI boresighted on the Walkway.

    Anyhow, none of the Baofeng squelch settings had any effect, which turned out to be a known problem. The default range VHF covered a whopping 6 dB and the UHF wasn’t much better at 18 dB, both at very low RF power levels.

    We use the radios in simplex mode, generally within line of sight, so I changed the Service Settings to get really aggressive squelch:

    Baofeng UV-5R - Improved Squelch Settings
    Baofeng UV-5R – Improved Squelch Settings

    I have no way to calibrate the new signal levels, but I’d previously cranked the squelch up to 9 (it doesn’t go any higher) and, left unchanged, the new level makes all the previous interference Go Away™. Another ride over the Walkway with the squelch set to 4 also passed in blissful silence.

    If the BF-F9 levels mean anything on a UV-5R, that’s about -100 dBm, 20 dB over the previous -120 dBm at squelch = 9.

    The new squelch levels may be too tight for any other use, which doesn’t matter for these radios. As of now, our rides are quiet.

    [Update: Setting the squelch to 5 may be necessary for the Walkway, as we both heard a few squawks and bleeps while riding eastbound on a Monday afternoon. ]

  • Exhibit Hand-Out Cards: QR Version

    I’ve finally had it beaten into my head: any public exhibition requires paper handouts, if only for younger folks who are too shy to ask questions. Paper may seem obsolete, but it serves as a physical reminder long after the sensory overload of a busy event fades away.

    Hence, I made up cards describing my exhibits at the HV Open Mad Science Fair, each sporting a QR code aimed at far more background information than anybody should care about:

    Mad Science Fair - handout cards
    Mad Science Fair – handout cards

    The QR codes come from one-liners:

    qrencode https://softsolder.com/?s=dso150 -s 5 -d 300 -o dso150.png

    So, go ahead, shoot ’em with your phone:

    • Blog search QR code: astable
    • Blog search QR code: bowl-of-fire
    • Blog search QR code: dso150
    • Blog search QR code: halogen
    • Blog search QR code: hp7475a
    • Blog search QR code: tubes

    Memo to Self: put the cards in the Big Box o’ Stuff the night before.

  • Astable Multivibrator Blinkies: Radome Attachment

    Ping-Pong ball radomes tend to fall off their perches at the slightest touch:

    RGB LED - radome test
    RGB LED – radome test

    Because I planned to take my collection along to HV Open’s Mad Science Fair, I finally used a Round Tuit for some adhesive action.

    The general plan was to punch a ring from double-sided tape, thusly:

    Astable - Radome adhesive - poor surface
    Astable – Radome adhesive – poor surface

    The OD required touching up the edge of a brass tube punch I’d made a while ago:

    Astable - Radome adhesive - punch sharpening
    Astable – Radome adhesive – punch sharpening

    It worked exactly as expected:

    Astable - Radome adhesive - punching
    Astable – Radome adhesive – punching

    Unfortunately, the 3D printed spider’s “spherical” socket has such a rough surface that the adhesive had too few contact points to hold the ball in place.

    My fallback has become 3M outdoor-rated double-stick foam tape, so:

    Astable - Radome adhesive - 3M foam tape
    Astable – Radome adhesive – 3M foam tape

    This leaves a small black ring visible between ball and socket. Recessing the foam tape by half its thickness should improve its ahem optics, although it’s probably not worth the effort with black PETG.

  • Shower Curtain Magnet Anchors

    Back in the day, bathtubs had a porcelain coating over a cast-iron carcass, so embedding little magnets in shower curtains worked perfectly to keep the loose ends from billowing out of the tub. Surprisingly, even here in the future, with plastic bathtubs ruling the land, some shower curtains still have magnets. The mud-job tile walls of shower stall in the Black Bathroom have nary a trace of iron, but we though I could add ferrous targets for a new shower curtain, thusly:

    Shower Curtain Anchor - installed
    Shower Curtain Anchor – installed

    The magnet lives inside a heat-sealed disk, so it’s (more-or-less) isolated from the water. As you’d expect, it’s a cheap ceramic magnet, not a high-performance neodymium super magnet, with no more strength than absolutely necessary to work under the most ideal of conditions.

    My anchors must also be waterproof, firmly attached, non-marking, easily removable, and no more ugly than absolutely necessary. The general idea is to slice the bottom from a pill bottle, entomb a thin steel disk in epoxy, and attach to the tile with a patch of outdoor-rated foam tape.

    So, we begin …

    Cutting a narrow ring from a pill bottle requires a collet around the whole circumference, which started life as some sort of stout aluminum pole:

    Shower Curtain Anchor - cutting tube stock
    Shower Curtain Anchor – cutting tube stock

    Bore out the inside, with a small step to locate the bottle:

    Shower Curtain Anchor - boring fixture
    Shower Curtain Anchor – boring fixture

    Clean up the outside, just for pretty:

    Shower Curtain Anchor - turning fixture OD
    Shower Curtain Anchor – turning fixture OD

    Slit the fixture to let it collapse around the bottle, then chuck up the first victim with support from a conveniently sized drill chuck in the tailstock:

    Shower Curtain Anchor - cutting bottle
    Shower Curtain Anchor – cutting bottle

    I did a better job of cutting the second bottle to the proper length:

    Shower Curtain Anchor - parting base
    Shower Curtain Anchor – parting base

    Nibble disks from sheet metal, half-fill the bottle bottoms with steel-filled (and, thus, magnetic!) JB Weld epoxy, insert disks, add sufficient epoxy to cover the evidence:

    Shower Curtain Anchor - epoxy curing
    Shower Curtain Anchor – epoxy curing

    Fast-forward to the next day, punch out two disks of double-sided foam tape:

    Shower Curtain Anchor - adhesive foam
    Shower Curtain Anchor – adhesive foam

    Affix, install, and it’s all good.

    Actually, it’s not. The ceramic magnets are so weak they don’t hold the curtain nearly well enough to satisfy me. The next anchor iteration should have embedded neodymium magnets to attract the curtain’s crappy ceramic magnets, but this is Good Enough™ for now.

  • Kinesis Freestyle 2: Steel Tactile Bumps

    Adding tape bumps to the worn Kinesis keyboard demonstrated I really need tactile home keys, so I popped the tops and fired up the Sherline mill:

    Kinesis keyboard - 2 mm drilling
    Kinesis keyboard – 2 mm drilling

    That’s a genuine 2 mm carbide end mill, poked 1 mm into the key cap, snuggled right up against the front edge.

    Two epoxy dabs and some wiping later:

    Kinesis keyboard - 2 mm tactile bearings
    Kinesis keyboard – 2 mm tactile bearings

    The careful alignment on the F key tells you I did it first; obviously, I should make better fixtures.

    The holes could be slightly larger and maybe slightly deeper, but the bearings feel just right.

    Indeed, they work so well a ball now distinguishes the far-flung Delete and Backspace keys:

    Kinesis keyboard - 2 mm bearing - Delete key
    Kinesis keyboard – 2 mm bearing – Delete key

    Now, to see how long the epoxy lasts …

  • Mini-Lathe Cut-Off Tool Holder: Improved Clamp Screw

    Apparently all mini-lathe cutoff tool holders suffer from the same problem:

    Lathe Cutoff Tool - OEM swaged screw
    Lathe Cutoff Tool – OEM swaged screw

    The clamp tightening screw is made from butter-soft Chinese steel with a swaged hex socket. As you’d expect, the hex wrench eventually (as in, after a few dozen adjustments, tops) rips the guts right out of the socket.

    The screw has a M6×1.0 mm threads, but the thread around the hex recess is left-handed. While I could, in principle, print a 127 tooth change gear, rebuild the lathe’s banjo to accommodate it, then single-point a backassward M6 thread, it’s easier to just use a standard socket head cap screw:

    Lathe Cutoff Tool - rebuilt screw
    Lathe Cutoff Tool – rebuilt screw

    The clamp screw passes through the block at an angle:

    Lathe Cutoff Tool - blade view
    Lathe Cutoff Tool – blade view

    Fortunately, the screw is perpendicular to the angled side over on the left, making it easy to clamp in the Sherline’s vise:

    Lathe Cutoff Tool - aligning to screw
    Lathe Cutoff Tool – aligning to screw

    Using the laser aligner seemed like a good idea at the time, but the top of the screw wasn’t particularly well-centered on the hole’s axis. I couldn’t screw the left-hand part (with the socket) in from the bottom and center the block near its surface, because then I couldn’t extract the screw before proceeding.

    I used a diamond burr to grind out a flat for the screw head:

    Lathe Cutoff Tool - clearing screw recess
    Lathe Cutoff Tool – clearing screw recess

    The flat came from about twenty manual G2 I-2.5 full-circle passes, stepping down through the hard steel block 0.1 mm per pass, at a too-slow 4000 RPM and a too-fast 30 mm/min feed, with plenty of water squirted from one side into a shop vac snout on the other. The doodle in the background of the first picture shows a first pass at the layout, with the burr centered at X=-2.5; I actually did the grinding from X=+2.5 so most of the passes started in thin air.

    The screw head started just shy of 10 mm OD and the burr just over 5.2 mm, so the ensuing 5 mm circles created a flat barely large enough. If the flat were perfectly centered on the screw axis, I wouldn’t have had to grind out another millimeter on the left side (toward the bottom of the tool holder body), but it worked out OK:

    Lathe Cutoff Tool - 6 mm SHCS test fit
    Lathe Cutoff Tool – 6 mm SHCS test fit

    The trial fitting also showed the head stuck out ever so slightly beyond the far side of the block, where it would interfere with the blade, so I turned off 0.4 mm off its OD.

    If I had a 50 mm SHCS in hand, I’d have used it. Instead, I extended the threads of a 75 mm screw, then lopped off the end to the proper length. I’ll spare you the ordeal, including the moment when I reached for the cutoff tool to shorten the screw. A bag of such screws will arrive shortly, in preparation for future need.

    Now the [deleted] cut-off holder works the way it should have from the beginning.

  • MPCNC: Calculating Spring Rates

    Calculate the spring rates for the drag knife, diamond engraver, and collet pen holders by measuring the downforce every 0.5 mm (or so):

    LM12UU Collet Pen Holder - spring rate test
    LM12UU Collet Pen Holder – spring rate test

    Then plotting the data points and eyeballing a straight-line curve fit:

    MPCNC - Drag Knife Holder - spring constant
    MPCNC – Drag Knife Holder – spring constant

    Doing it on hard mode definitely has a certain old-school charm. The graph highlights mis-measured data and similar problems, because, if you don’t see a pretty nearly straight line, something’s gone awry.

    But we live in the future, so there’s an easier way:

    Droid48 - Spring Rate - Linear Fit coefficients
    Droid48 – Spring Rate – Linear Fit coefficients

    Well, OK, it’s the future as of the early 1990s, when HP introduced its HP 48 calculators. I’m using the Droid48 emulator on my ancient Google Pixel: living in the past, right here in the future.

    Start by firing up the STAT library (cyan arrow, then the 5 key), selecting Fit Data … from the dropdown list, then selecting the Linear Fit model:

    Droid48 - Spring Rate - Linear Fit screen
    Droid48 – Spring Rate – Linear Fit screen

    Then tap EDIT and enter the data in a tiny spreadsheet:

    Droid48 - Spring Rate - Linear Fit data
    Droid48 – Spring Rate – Linear Fit data

    My default “engineering mode” numeric display format doesn’t show well on the tiny screen. Tapping the WID→ key helps a bit, but shorter numbers would be better.

    With the data entered, set an X value and tap the PRED key to get the corresponding Y value:

    Droid48 - Spring Rate - Linear Fit prediction
    Droid48 – Spring Rate – Linear Fit prediction

    Tapping the OK button puts the line’s coefficients on the stack, as shown in the first picture. Write ’em on a strip of tape, stick to the top of the holder, and it’s all good:

    LM12UU Collet Pen Holder - test plot - overview
    LM12UU Collet Pen Holder – test plot – overview

    Works for me, anyhow.

    HP still has the HP 48g manuals online. The (unofficial) HP Museum has a page on the HP 48S. More than you want to know about the 48 series.