The Smell of Molten Projects in the Morning

Ed Nisley's Blog: Shop notes, electronics, firmware, machinery, 3D printing, laser cuttery, and curiosities. Contents: 100% human thinking, 0% AI slop.

Tag: Improvements

Making the world a better place, one piece at a time

  • Bathroom Sink Stopper Rod

    After swapping the corroded steel rod end-for-end twice, I expected this would happen:

    Bathroom Sink Stopper Rods
    Bathroom Sink Stopper Rods

    So now we know a chrome-plated steel rod will survive 16 years in a bathroom drain, at least if you’re willing to coddle the fool thing far more than seems reasonable.

    I eased a slug of epoxy into the brass tube to seal the wet end. Given how little use the stopper gets, I hope it lasts forever …

  • More Tommy Bar Handles

    Having used a nail for far too long, this is a definite step up for my machinist vises:

    Tommy Bar - machinist vise
    Tommy Bar – machinist vise

    The vise knob has a hole just barely passing a length of 3.4 mm = 9/64 inch mild steel rod from the Small Box o’ Cutoffs.

    While I was at it, I made a handle for the parallel jaw clamps:

    Tommy Bar - parallel jaw clamp
    Tommy Bar – parallel jaw clamp

    Those knobs pass a 3.0 mm = 1/8 inch rod, similarly sourced. Inexplicably, one clamp expected no more than a 7/64 inch rod; a brief introduction to Mr Drill Press persuaded it concerning the error of its ways.

    I should have made the handles distinctively different, because they’ll get mixed up in the box of vises & clamps. Next time, fer shure!

    The Tommy Bar handles use the same solid model as the Sherline Tommy Bars, with hole diameters as noted. Cyan PETG is definitely easier on the eye than red PLA, although it does fade into the background clutter around here.

  • Sunglass Earpiece Trimming

    Mary doesn’t like wearing the wrap-around-her-head earpieces found on sunglasses these days under her bicycle helmet, so I must trim them to fit:

    Sunglass earpiece trim
    Sunglass earpiece trim

    Perhaps I won’t need an old pair to prepare the next set: a scant four inches from the hinge.

  • Cheese Slicer: XTC-3D Epoxy Coating

    We have, as you might expect, a Favorite Cheese Slicer of no particular provenance. Being made of cheap pot metal, it left black smudges wherever it went and, decades ago, I coated it with bright red rubbery grip material. Recently, the coating became lumpy and peeling off the loose sections revealed a definite problem:

    Cheese slicer - aluminum corrosion
    Cheese slicer – aluminum corrosion

    Vigorous scrubbing with a foam sanding block and a Scotchbrite pad, interspersed with rotary wire brushing, removed the corrosion and left a slightly pitted metal frame. Protip: scrub under water and wire-brush with a vacuum hose to keep the dust under control.

    A pair of 6-32 screws, nuts, and brass sleeves, with two oil dots protecting the frame threads, provided hand grips while I wiped it down with denatured alcohol and coated it with XTC-3D epoxy:

    Cheese slicer - epoxy curing
    Cheese slicer – epoxy curing

    Turns out the mixing stick worked quite well to cover the entire thing, as the epoxy does a great job of leveling itself. I suppose wasting a tiny brush would be more professional, but …

    It quietly dripped excess epoxy into a strategically placed trash can for about ten minutes. I wiped off the final drip before the epoxy solidified, leaving a smooth layer over the end of the handle:

    Cheese slicer - reassembled
    Cheese slicer – reassembled

    It’s back in service and works as well as ever, with a handle now smooth to the touch. I suppose I could have tinted the epoxy to hide the metal, but we regard those corrosion pits as beausage.

    I’ve slathered XTC-3D on some 3D printed parts, but have no idea how durable it is; this should serve as an accelerated survival test under rather harsh usage.

    The instruction sheet says XTC-3D isn’t the most transparent epoxy they make and, indeed, the layer left in the mixing pan came out more hazy than I expected:

    XTC-3D Epoxy - thin cured layer
    XTC-3D Epoxy – thin cured layer

    They point out the haze doesn’t matter for thin surface coatings, which is certainly true.

  • Whirlpool Refrigerator Drawer Slide: Another Bracket

    Thirteen years after the original repair on the left side and eight years after I fixed the drawer slide on the right side, this happened:

    Refrigerator shelf slide - failed parts
    Refrigerator shelf slide – failed parts

    The general idea is to wrap a new bracket around the old bracket, because trying to remove the old one will probably cause more damage:

    Refrigerator shelf slide - trial assembly
    Refrigerator shelf slide – trial assembly

    A pair of screws hold the new bracket to the shelf support:

    Refrigerator shelf slide - support screw nut openings
    Refrigerator shelf slide – support screw nut openings

    Those two screws must support the entire weight of the drawer, which is exactly what broke the original all-plastic frame and slide.

    The epoxy chip and transparent plastic sheet in the first picture spaced the old aluminum bracket away from the shelf support and reduced the space beyond the new bracket enough to require drilling access holes. Fortunately, they’re hidden inside the support frame, so nobody will ever know.

    The shelf support is a huge floppy rectangle, so I clamped it to the bench vise while drilling the holes:

    Refrigerator shelf slide - upright vise clamp
    Refrigerator shelf slide – upright vise clamp

    The new bracket is on the right, with a sheet of white acrylic spacing it away from the shelf support by exactly the same distance as the angled aluminum snippet replacing the failed epoxy & plastic on the broken part:

    Refrigerator shelf slide - bracket parts
    Refrigerator shelf slide – bracket parts

    The two holes in the middle of the aluminum parts show that I used exactly the same angle brackets as raw material. It’ll be a sad day when I eventually use the last of those brackets.

    Putting the parts together, with double-stick tape holding all the parts in place, shows how they fit:

    Refrigerator shelf slide - repair trial assembly
    Refrigerator shelf slide – repair trial assembly

    And then it just snapped into place. I didn’t bother pretending solvent glue would help anything, nor did I apply any epoxy, so this whole thing hangs from those two 4-40 screws. On the other paw, their steel beats the original white plastic.

    I devoutly hope to never rebuild the actual drawer slide, but these dimensions may help somebody else out of a jam:

    Refrigerator shelf slide - dimensions
    Refrigerator shelf slide – dimensions

    The vertical “40” dimension refers to the available space from the bottom of the white plastic part to the top of the shelf support frame; the new bracket is a tad shorter than that.

    The plastic parts in that refrigerator have been a complete disappointment: were it not for my relentless repair jones, we’d likely be on our third or fourth refrigerator by now. Oddly, the cooling parts continue to chug along (*), without more than the occasional loud noise in the middle of the night.

    We’re definitely doing our part to reduce our waste stream.

    (*) The most recent freezer fan hasn’t failed yet!

  • 60 kHz Preamp: Filtering and Rebiasing

    The LT1920 instrumentation amplifier now sports two silver-mica caps on its inputs as a differential-mode input filter cutting back strong RF signals (clicky for more dots):

    60 kHz Preamp Schematic - DM filter inst amp - BP filter rebias - 2017-09-22
    60 kHz Preamp Schematic – DM filter inst amp – BP filter rebias – 2017-09-22

    In principle, a DM filter should eliminate RF rectification from out-of-band signals, although I think the attic is quiet enough to not need any help. The caps form a simple RC LP filter rolling off at 5.490 kΩ × 150 pF → 193 kHz, high enough above the 60 kHz signal to not make much difference down there.

    The silver-mica caps come from the Big Box o’ Caps, which contained an envelope with a few large 150 pF ±1% caps and a bag stuffed with similar 147 pF ±1% caps. Mixed in with the latter were some smaller 147 pF caps (*) of no particular tolerance (perhaps 5%), from which I neurotically matched a pair to 0.05 pF without too much effort. Doesn’t matter, given the other tolerances and suchlike, but it was amusing.

    I’d inadvertently grounded the cold end of the 330 Ω input resistor in the LM353 bandpass filter, now properly tied at the Vcc/2 virtual ground to take the DC load off the LT1920 output: a 100 nF cap (27 Ω at 60 kHz) stores the bias level without messing up the filter shape.

    A similar cap rebiases the protected resonator at the LT1010 buffer input:

    60 kHz Preamp Schematic - protected resonator - output rebias - 2017-09-22
    60 kHz Preamp Schematic – protected resonator – output rebias – 2017-09-22

    The new caps aren’t all that visible and the resonator vanishes in the clutter:

    60 kHz Preamp - protected resonator filter - overview
    60 kHz Preamp – protected resonator filter – overview

    Next: find out how well it works!

    (*) Yes, there were two envelopes between 150 pF and 147 pF:

    Silver-mica caps
    Silver-mica caps
  • 60 kHz Preamp: Power LED Resistor Oops

    I eventually noticed the yellow LED indicating +24 V input from the power supply (previously, a noisy wall wart) was dark. Poking around revealed I’d inadvertently installed a 1 kΩ ballast resistor:

    LF Preamp - burned power-on LED resistor
    LF Preamp – burned power-on LED resistor

    A 1/4 W resistor can’t dissipate half a watt for very long, as shown by the discolored circuit board around the leads and the faint smell of electrical death in the area.

    I swapped in a 3.3 kΩ resistor, the yellow LED lit up for a few seconds, then went dark again. This time, the LED was dead; apparently, it’d been overstressed for long enough to fail. I can’t be too annoyed.

    Unfortunately, replacing the LED required removing the entire housing with all three LEDs, chopping off the defunct block, reinstalling the attenuated block with the two green LEDs, installing a similar red LED, and finally installing a nice 3.3 kΩ half-watt resistor:

    Power LED - Red with 0.5 W resistor
    Power LED – Red with 0.5 W resistor

    So it goes …