The Smell of Molten Projects in the Morning

Ed Nisley's Blog: Shop notes, electronics, firmware, machinery, 3D printing, laser cuttery, and curiosities. Contents: 100% human thinking, 0% AI slop.

Tag: Repairs

If it used to work, it can work again

  • Vacuum Tube LEDs: Knockoff Arduino Nano USB Connector

    The LEDs adorning the 0D3 rectifier tube became unreliable:

    0D3 Octal - 25 mm socket - raised LED
    0D3 Octal – 25 mm socket – raised LED

    After failing to plug in a different USB power supply, a close look at the USB connector showed the problem:

    Knockoff Arduino Nano - broken Mini-B connector
    Knockoff Arduino Nano – broken Mini-B connector

    A bit of needle-nose tweezering extracted the culprit from the power supply’s connector:

    Knockoff Arduino Nano - broken Mini-B connector - fragment
    Knockoff Arduino Nano – broken Mini-B connector – fragment

    I tried applying the world’s smallest dot of epoxy to the fracture, probably slobbered epoxy along the pins while reinserting it, and the Nano still doesn’t light up.

    Given that knockoff Nano boards cost a touch over two bucks delivered, it’s not clear transplanting a connector from one of the never-sufficiently-to-be-damned counterfeit FTDI USB adapters makes any sense.

  • Byonics TinyTrak3+ vs. RFI

    Some weeks ago, the APRS + voice adapter on my radio began randomly resetting during our rides, sending out three successive data bursts: the TinyTrak power-on message, an ID string, and the current coordinates. Mary could hear all three packets quite clearly, which was not to be tolerated.

    I swapped radios + adapters so that she could ride in peace while I diagnosed the problem, which, of course, was both intermittent and generally occurred only while on the road. The TinyTrak doc mentions “… a sign of the TinyTrak3 resetting due to too much local RF energy”, so I clamped ferrite cores around All! The! Cables! and the problem Went Away.

    Removing one core each week eventually left the last core on the GPS receiver’s serial cable, which makes sense, as it plugs directly into the TT3. The core had an ID large enough for several turns (no fool, I), another week established a minimum of three turns kept the RFI down, so I settled for five:

    KG-UV3D APRS - ferrite on TT3 GPS cable
    KG-UV3D APRS – ferrite on TT3 GPS cable

    Prior to the RFI problem cropping up, nothing changed. Past experience has shown when I make such an assertion, it means I don’t yet know what changed. Something certainly has and not for the better.

    I swapped the radios + adapters and all seems quiet.

  • Layout Pen For Black Objects

    This worked surprisingly well to lay out black foam gaskets for new fairing mounting plates:

    Black foam layout with ceramic fabric pen
    Black foam layout with ceramic fabric pen

    Mary uses the Fons & Porter Mechanical Pencil to mark quilting patterns on fabric. It has, they say, a “strong ceramic 0.9MM white lead” with “water-soluble dyes” capable of both laying down a durable mark and washing out without leaving a trace. I don’t care about the latter, of course, but it did brush off reasonably well.

    The next step involved running an X-Acto knife around the perimeter of the plate and punching the holes.

    You can get colored ceramic leads (for small values of color) for use on other backgrounds.

  • HP 7475A Plotter: Rebuilt Carousel Drive

    A followup to the saga of the HP 7475A plotter with a broken carousel drive:

    With the information you shared, we were able to successfully model and reconstruct the drive wheel in only a couple of days.

    One useful thing we discovered is there’s a lot of room for error – so long as the pin catches and the wheel isn’t slipping on the motor shaft, the mechanism will work. The grooves and the interior radius of the original part aren’t critical.

    Because of your heads up about Geneva wheels, I found this excellent website – https://newgottland.com/2012/01/08/make-geneva-wheels-of-any-size/ – which includes a link to a Geneva wheel calculator. With the measurements you sent and a measurement off of the pen carousel, the calculator generated near perfect dimensions for a replacement. There was a little sanding and rounding to fit but it was certainly within tolerance.

    Interestingly, the pieces of the drive wheel that I pulled out of the case revealed a small hidden detail. On the underside, there’s a collar around the motor shaft that gives the cam an extra ~.03″ thickness. Presumably this is to help reduce friction during travel. Our prototype doesn’t take this detail into consideration – we’ve had no issues with friction, and we compensated for the thickness by making the pin a little longer – but it’s meaningful to note.

    HP7475A Carousel Drive - cam1
    HP7475A Carousel Drive – cam1

    The broken pieces also confirmed the thicknesses and radii of the original part, and so my partner was able to build an accurate technical drawing of the drive wheel for future fabrication.

    While we intend to make a better replacement, our prototype was built with dense 1/8″ mat board, PVA glue, binder clips, and a short piece of wooden dowel from our bits box. Basically just stuff we had kicking around the studio. It’s held up shockingly well. A little dented around the edges from hitting the carousel, but there’s no slippage. I’m thinking I’ll use it until it falls apart, just to see how long it takes.

    HP7475A Carousel Drive - repaired - cam2
    HP7475A Carousel Drive – repaired – cam2

    Attached, find a technical drawing comparing the original drawing to our prototype (measured in good old fashioned 1980s inches); a photo of the retrieved piece, showing the collar on the reverse side; and a photo of the prototype in place. Feel free to share these – everyone deserves a working plotter!

    7475a drive wheel
    7475a drive wheel

    Once the carousel was working, my roommate – an electrical engineer – hooked me up with a custom serial cable, a Raspberry Pi, and a crash course in Python, so now that I can communicate with the plotter, the possibilities are staggering. I’m thrilled to add this machine to my print studio arsenal!

    I love a happy ending …

    For anyone with a new-to-you plotter, search the blog for 74754A to find info on replacing failed electrolytic capacitors, adapting Sakura Micron pens, refilling old plotter pens, building a serial cable, hacking Chiplotle to actually use hardware handshaking, and plotting Superformulas. Let me know how you got your plotter working!

  • Tour Easy: White ABS vs. Six Years of Sunlight

    These white ABS fairing plates held the Zzipper fairing on my Tour Easy ‘bent since 2011:

    ABS Fairing Plates - 6 years
    ABS Fairing Plates – 6 years

    Over the course of those six years I’ve ridden about 6 × 2500 = 15000 miles, maybe more, maybe less. I can ride at 15 mph for a while, but 12 mph seems a more reasonable overall estimate, making for a bit over 1000 hours. Figure the bike spends that much time sitting outdoors at the far end of the ride and you’re looking at what 2000+ hours of sunlight does to ABS.

    In addition to discoloration, the plates have become brittle, as shown in the chips in third one down, and permanently deformed due to the pressure of the nylon bolts compressing the black foam against the fairing.

    A closer look at the top plate:

    ABS Fairing Plates - 6 years - detail
    ABS Fairing Plates – 6 years – detail

    My 3D print quality has improved a lot since then.

    New plates of a different design are, as NASA puts it, “in work”.

    The pix come from the new LiDE 120 scanner. It does a good job with the color, but has (for good reason) an essentially zero depth of field: if it’s not on the glass, it’s out of focus.

  • Optiplex 980 Power Supply: Capacitor FAIL

    Came up from the Basement Laboratory to find my Dell Optiplex 980 PC had failed, with the power button and diagnostic 1 + 3 LEDs blinking amber. They built it back in June 2010, so section 3 of the Dell reference applies, the power supply status LED on the back panel was off, and, going straight to the heart of matter, I popped the top, disconnected the internal power supply cables, and poked the power supply test button:

    Optiplex 980 Power Supply - rear panel test button
    Optiplex 980 Power Supply – rear panel test button

    … and it’s dead.

    Inside, the system board sports a Mini-ATX power supply connector:

    Optiplex 980 - Mini-ATX power connector
    Optiplex 980 – Mini-ATX power connector

    I originally hoped to swap a supply from an Optiplex 755 (also in a Small Form Factor case) residing on the recycle heap, but it has an ordinary ATX connector:

    Optiplex 755 - ATX power connector
    Optiplex 755 – ATX power connector

    So I moved the 980’s SSD and dual-Displayport video card into the 755, fired that devil up, and … it worked!

    With my desktop back in action, albeit somewhat slower, I popped the dead supply’s case by violating the Warranty Void If This Label Removed sticker to unscrew the last screw:

    Optiplex 980 Power Supply - overview
    Optiplex 980 Power Supply – overview

    Notice anything?

    The electrolytic capacitors over on the left look like this:

    Optiplex 980 - Good capacitor
    Optiplex 980 – Good capacitor

    The cluster of caps on the upper right have bulged pressure-relief lids, like this:

    Optiplex 980 - Bulging capacitor 1
    Optiplex 980 – Bulging capacitor 1

    And this:

    Optiplex 980 - Bulging capacitor 2
    Optiplex 980 – Bulging capacitor 2

    And this:

    Optiplex 980 - Bulging capacitor 3
    Optiplex 980 – Bulging capacitor 3

    None had ruptured, but they’re obviously feeling a bit nauseous.

    Given the 980’s mid-2010 manufacturing date, this probably isn’t capacitor plague, just simple overheating from operating in a dead-air zone amid all those heatsinks and wires. Some of the Usual Unnamed Sources suggest overheating the capacitors is how manufacturers ensure their hardware doesn’t last forever, without being obvious about planned obsolescence; I’m loathe to ascribe to malice what can be explained by design desperation.

    A Genuine Dell replacement supply from eBay ($25 delivered) came from yet another “small form factor” Dell chassis, so it isn’t quite the same size, lacks a supply test button / LED status light, and doesn’t quite fit:

    Optiplex 980 - replacement supply misfit
    Optiplex 980 – replacement supply misfit

    Nothing a sheet metal nibbling tool can’t fix, though, given I haven’t developed a deep emotional attachment to the chassis. I gnawed off the left side of the frame and squared up the rim around the lower screw, after which the opening fit the supply pretty well, although the latching tab bent up from the bottom of the chassis didn’t quite engage the far end of the supply. No big deal: it’s not in a high-vibration environment.

    The new-to-me supply also carries an ATX connector, but the eBay seller included a Mini-ATX adapter. Jamming the adapter + wires into the space available required concerted muttering, assisted by tucking the SSD under the DVD-RW drive. No pictures, as it’s a classic seven pounds in a five pound box situation.

    And then It Just Worked again.

  • Amazon EK3211 Scale: Re-Footing

    Our long-suffering kitchen scale lost a pair of feet, most likely because those two feet do most of the skidding as we slide it onto a shelf below a cabinet. The scale has (well, had) six silicone rubber feet:

    Amazon EK3211 Scale - OEM foot
    Amazon EK3211 Scale – OEM foot

    The vagaries of color photography turned a neutral-gray silicone disk into that weird blue.

    A pair of ¼ inch disks punched from non-skid textured rubber tape fit perfectly into the recesses:

    Amazon EK3211 Scale - tread foot
    Amazon EK3211 Scale – tread foot

    Now, we’ll see how tread adhesive withstands the same abuse.