The Smell of Molten Projects in the Morning

Ed Nisley's Blog: Shop notes, electronics, firmware, machinery, 3D printing, laser cuttery, and curiosities. Contents: 100% human thinking, 0% AI slop.

Tag: Repairs

If it used to work, it can work again

  • Taylor 1478 Kitchen Thermometer: Probe Wire Failure

    We’ve been doing a lot of roasting and bought a not-dirt-cheap Taylor 1478 digital kitchen thermometer with a long probe wire to monitor the meat temperature. As soon as I unpacked it, I knew this would eventually happen:

    Kitchen thermometer - nicked probe wire
    Kitchen thermometer – nicked probe wire

    The cable lasted just long enough to ensure the thermometer warranty expired; it’s a deliberate design flaw if I’ve ever seen one.

    The thermistor inside the probe seems to be 100 kΩ at ordinary temperatures, although I’d be completely unsurprised to find that Taylor uses a slightly nonstandard resistance. Because nonstandard, of course.

    Anyhow, replacement probes (*) are readily available from the usual Amazon suppliers, feature stainless steel braid sheathing and cost about as much as a whole new thermometer (albeit those still have cheap plastic insulation). With a replacement on order, I hauled the failed probe to the shop for an autopsy and possible resurrection…

    Although I hoped that hammering out the crimp would release the thermistor, it was not to be. In retrospect, pulling on the probe wire probably killed it, but I didn’t know that at the time.

    A spring intended to stabilize tubing while bending worked just fine to un-bend the probe:

    Kitchen thermometer - unbending
    Kitchen thermometer – unbending

    But, alas, the thermistor still didn’t emerge from the more-or-less straightened probe.

    Some deft work with a Dremel cutoff wheel sliced enough off the stainless steel tube that I could splice the wires:

    Kitchen thermometer - probe cutting
    Kitchen thermometer – probe cutting

    More cutoff wheel work smoothed the edges of that raw cut end, although the result wasn’t anything to show off.

    The spliced and insulated probe definitely don’t win any awards, either:

    Kitchen thermometer - probe rebuild
    Kitchen thermometer – probe rebuild

    I doubt that the heatshrink tubing or silicone wrap underneath it would be suitable for roasts in the kitchen, but that’s moot: the probe remained intermittent.

    If the new probe is also intermittent, then I’ll suspect the crappy 2.5 mm jack in the side of the thermometer…

    (*) It’s not clear that a replacement probe for a 1470N thermometer will work with a 1478 thermometer. I’m gambling that Taylor wouldn’t be so stupid annoying deliberately obtuse as to use different probe thermistors, but that’s surely a bad bet. There’s no reason to believe Taylor actually makes any of this stuff, which means different models may come from entirely different designers / factories with entirely different supply chains.

  • Incremental Architecture

    The nice countertop and sinks look like obvious replacements since they built this rest area on the NYS Northway up near Saratoga. Unlike the old sinks, however the countertop needed support struts to prevent the backsplash from peeling off the wall when somebody leans on the edge and those struts required planks to make the spacing work out:

    NYS Northway Rest Room - Sink Supports
    NYS Northway Rest Room – Sink Supports

    Too bad about that strut right where the drain cleanout plug emerges from the wall. Also too bad that the elaborate welded square doesn’t rest on the wall, so it’s not really supporting anything. Triply too bad about the trim plate that used to conceal the plug; the one that didn’t fit behind the square.

    Also: why do the sink drains have such a long horizontal run between the drain tailpiece and the trap? Maybe that’s so they can retrieve rings and other valuables that go down the drain? Perhaps the other trap orientation would put the joint too far forward, where it can be dislodged by an errant knee?

    I’ve certainly created incremental monstrosities like that; look no further than the successive APRS interfaces on our bikes

  • Hotrod M2 Platform Support Stud Repair

    The hotrod build platform I’m using with the Makergear M2 consists of a PCB heater bonded to a glass plate, supported by three socket head cap screws soldered into the PCB. The print quality recently took a nosedive that seemed related to the first layer height, with which I fiddled more than usual, and finally the front of the platform became obviously, visibly, no-way-around-it far too high. Peering under the platform showed that the front support stud had pulled out of the solder fillet securing it to the PCB:

    M2 Hotrod Platform - support stud pullout
    M2 Hotrod Platform – support stud pullout

    Those PCB patterns conduct the heater current around the mounting holes: the hotrod platform has better heat distribution than the OEM M2 platform.

    The offending screw didn’t go anywhere:

    M2 Hotrod Platform - support stud in spring
    M2 Hotrod Platform – support stud in spring

    The wavy spring and silicone plug press on the PCB, so the solder fillet had to support all the stress. It seemed as though the solder hadn’t bonded to the stainless SHCS, but, rather than try to fix that, I decided to put a washer on the screw. That way, the spring bears on the washer and the screw head supports the strain, with the solder fillet responsible for holding the PCB and glass plate in position.

    Alas, I didn’t have any washers small enough on the inside (3 mm) and big enough on the outside to support the springs, so I cut some out of a sheet steel scrap by drilling the center hole to the proper diameter, then applying a hole saw without its (far too large) pilot drill:

    M2 Hotrod Platform - hole-sawing washers
    M2 Hotrod Platform – hole-sawing washers

    That’s a lethally bad idea, as the pilot-less saw can grab the sheet and toss it across the shop. Notice the screws holding the sheet down and absorbing the cutting torque, plus the two clamps enforcing the “stay put” edict.

    The other problem with not having a pilot drill in the hole saw is that it’s not guaranteed to cut a cookie that’s concentric with the center hole. Instead of taking the time to make a pilot, I just drilled and cut a few extra washers, then picked the best three of the set for finishing:

    M2 Hotrod Platform - rough-cut washers
    M2 Hotrod Platform – rough-cut washers

    Using a screw as a mandrel, I lathe-turned the OD of the better ones to make them nice and round:

    M2 Hotrod Platform - washer on mandrel
    M2 Hotrod Platform – washer on mandrel

    Two of the three PCB support screws were in the right place (they hadn’t come loose), so I used the M2 as an alignment fixture for the third:

    M2 Hotrod Platform - aligning washers
    M2 Hotrod Platform – aligning washers

    That’s a layer of  good old JB Industro Weld epoxy, rated for much higher temperatures than the platform will ever see, between the big washers and the PCB. I buttered up the head of the errant screw and the inside of the solder fillet, shoved it in, and then stacked everything together. The small washers held the big washers perpendicular to the screws while the epoxy cured.

    After that, I removed the small washers, reinstalled springs + silicone plugs, tightened the nyloc nuts, aligned the platform, ran off a few thinwall hollow boxes, tweaked the alignment, and it was all good:

    M2 Hotrod Platform - thinwall box alignment
    M2 Hotrod Platform – thinwall box alignment

    The rest of the story: that mumble screw pulled loose on the Friday evening before the Mini Maker Faire on Saturday morning. I did all the shop work after supper, then let the epoxy cure overnight with the platform set to 95 °F while I got a good night’s sleep. Reinstalling and realigning the platform took the better part of half an hour around breakfast, after which I tore it all down, packed it all up, and headed off to the Mini Maker Faire.

    In truth, that’s the most trouble I’ve had with the M2 and it’s not Makergear’s fault: it’s not their platform. After reinstalling the platform, the alignment was no big deal and it’s been stable ever since.

  • Trust Multimedia Mouse: Gummy Rubber

    While looking for something else, I found the old Trust Multimedia Mouse and discovered its nice grippy rubber surfaces had become adhesive slime. Graduated efforts with water, rubbing alcohol, and denatured alcohol being unavailing, I finally hit it with xylene and that did the trick:

    Degummed Trust Mouse
    Degummed Trust Mouse

    Of course, xylene also wiped away the fancy button markings and irretrievably scarred the surface, but at least I can pick the mouse up without having it stick to my hand. Not that I pick it up that often, obviously.

    Several other gadgets have a similar grippy finish, so now I know what to do when it turns gummy: throw the gadgets out…

  • Eyeglass Temple Spring Repair

    Another of Mary’s glasses snapped at the temple joint:

    Broken eyeglass temple spring
    Broken eyeglass temple spring

    This one has a spring inside the joint that latches the temple on either side of that square inner corner. Obviously, there’s no way to reconnect the broken stub with the spring retracted inside the brazed temple box, so:

    • File off the corner
    • Fill the socket with epoxy
    • Ease the stub in place
    • Wipe off the excess epoxy
    • Align on the workbench
    • Let it cure overnight

    At least the hinge folds again, even if the spring doesn’t work:

    Broken eyeglass temple spring - epoxied
    Broken eyeglass temple spring – epoxied

    She promises to scrap out her oldest glasses after the next eye exam…

  • Heating Blanket Controller: Soldering QC

    A friend reported that three of the four heating blankets he’s bought over the last several years have failed, so he sent the lot to me for teardown and maybe repair.

    Looking inside one controller showed some obviously bad solder joints:

    Blanket controller - bad joints
    Blanket controller – bad joints

    Hitting the joints with the soldering iron improved their outlook on life, but the controller remained dead; they weren’t really bad joints, they just looked that way.

    If the “lot number” labels on the controllers mean anything, they’ve tried three different triac mounts over the years:

    • A through-hole triac screwed to the board with no heatsink
    • An SMD triac using the PCB copper as a heatsink
    • A through-hole triac with a big aluminum heatsink

    That’s in order of ascending lot number, suggesting the triac caused some reliability problems.

    I’m still trying to figure out how to probe the circuitry without killing myself. An isolation transformer comes to mind, because the blanket dissipates only 85 W.

    Surely the triacs have snubbers…

  • Shaft Position Sensor: Trimpot Wrench

    With the shaft position sensor mounted in this position:

    Kenmore 158 Shaft position sensor - overview
    Kenmore 158 Shaft position sensor – overview

    There’s no way to get a screwdriver into the trimpot that adjusts the sensor’s trip point.

    A few minutes with tin snips, nibbling tool, and square file produced a small wrench:

    Trimpot Wrench
    Trimpot Wrench

    One side of the wrench has a 45° bend that made tweaking the pot just slightly easier.

    The proper trip point turned out to be about 90° away from where the trimpot started, with the level midway between the detection points for shiny metal tape and the cutout side of the counterweight.