The Smell of Molten Projects in the Morning

Ed Nisley's Blog: Shop notes, electronics, firmware, machinery, 3D printing, laser cuttery, and curiosities. Contents: 100% human thinking, 0% AI slop.

Category: Machine Shop

Mechanical widgetry

  • Sony HDR-AS30V vs. Lithium Ion 18650 Cells

    These items came near enough to produce an irresistible force:

    Sony HDR-AS30V vs 18650 cells - side view
    Sony HDR-AS30V vs 18650 cells – side view

    How can you look at that layout and not jump to the obvious conclusion?

    The front view suggests enough room for a stylin’ case:

    Sony HDR-AS30V vs 18650 cells - end view
    Sony HDR-AS30V vs 18650 cells – end view

    You’d need only one cell for the camera; I happened to have two in my hand when the attractive force hit.

    The camera is 24.5 ⌀ x 47 tall x 71.5 overall length (67.8 front-to-door-seating-plane).

    The ATK 18650 cells are 19 ⌀ x 69 long, with the overlong length due to the protection PCB stuck on the + end of the cylinder. You can get shorter unprotected cells for a bit less, which makes sense if you’re, say, Telsa Motors and building them into massive batteries; we mere mortals need all the help we can get to prevent what’s euphemistically called “venting with flame“.

    Although I like the idea of sliding the cell into a tubular housing with a removable end cap, it might make more sense to park the cell over the camera in a trough with leaf-spring contacts on each end and a lid that snaps over the top. That avoids threaded fittings, figuring out how to get an amp or so out of the removable end cap contact, and similar imponderables.

    think it’s possible to drill a hole through the bottom of the camera at the rear of the battery compartment to pass a cable from a fake internal cell to the external cell. Some delicate probing will be in order.

    In round numbers, those 18650 cells allegedly have three times the actual capacity of the camera’s flat battery and cost about as much as the not-so-cheap knockoff camera cells I’ve been using.

  • Improvised Repairs Done Wrong

    Mary’s relatives encountered this repair in a rental flat during Thanksgiving week:

    Door handle - hex head bolt
    Door handle – hex head bolt

    Don’t have a hex bolt with the right thread? No problem: just use a sheet-metal screw, perhaps with a self-drilling point:

    Door handle - metal screw
    Door handle – metal screw

    Those hex heads let you apply more torque with less risk of stabbing yourself in the palm, which strikes me as an all-around Good Thing. I prefer socket-head cap screws, myself, but I’ll admit they’re an acquired taste.

    I’d like to think I wouldn’t do that …

  • J5-V2 700 lm Flashlight: QC FAIL, Redux

    The inside of the replacement J5 V2 Tactical Flashlight doesn’t have quite as much dirt on the LED emitter, but it’s still pretty bad:

    J5-V2 Flashlight - LED crud - second unit
    J5-V2 Flashlight – LED crud – second unit

    The small white dingus at about 10 o’clock seems to be a plastic shred stuck on end to the emitter lens. Here’s a better look, rotated a quarter-turn counterclockwise:

    J5-V2 Flashlight - LED crud detail - second unit
    J5-V2 Flashlight – LED crud detail – second unit

    There’s also an alien egg glued to the heatsink beside the LED:

    J5-V2 Flashlight - random pellet - second unit
    J5-V2 Flashlight – random pellet – second unit

    I’m hoping it’s another random plastic blob.

    There’s no point in returning this one; it’ll suffice for my purposes. However, given two random samples, I’d say the J5 Tactical Flashlight factory, wherever it may be in China, is really filthy.

    I’d hoped that paying a bit more for a “tactical” flashlight, instead of going bottom dollar, would yield a better product. Maybe it did?

  • Kenmore Progressive Vacuum Tool Adapters: Second Failure

    Pretty much as expected, the dust brush nozzle failed again, adjacent to the epoxy repair:

    Dust brush adapter - second break
    Dust brush adapter – second break

    A bit of rummaging turned up some ¾ inch Schedule 40 PVC pipe which, despite the fact that no plumbing measurement corresponds to any physical attribute, had about the right OD to fit inside the adapter’s ID:

    Dust brush - PVC reinforcement
    Dust brush – PVC reinforcement

    The enlarged bore leaves just barely enough space for a few threads around the circumference. Fortunately, the pipe OD is a controlled dimension, because it must fit inside all the molded PVC elbows / tees / caps / whatever.

    The pipe ID isn’t a controlled dimension and, given that the walls seemed far too thick for this purpose, I deployed the boring bar:

    Dust brush adapter - reinforced tube - boring
    Dust brush adapter – reinforced tube – boring

    That’s probably too much sticking out of the chuck, but sissy cuts saved the day. The carriage stop keeps the boring bar 1 mm away from the whirling chuck.

    Bandsaw it to length and face the ends:

    Dust brush adapter - reinforcement
    Dust brush adapter – reinforcement

    The PVC tube extends from about halfway along the steep taper from the handle fitting out to the end, with the section closest to the handle making the most difference.

    Ram it flush with the end:

    Dust brush adapter - reinforced tube - detail
    Dust brush adapter – reinforced tube – detail

    I thought about gluing it in place, but it’s a sufficiently snug press fit that I’m sure it won’t go anywhere.

    Natural PETG probably isn’t the right color:

    Dust brush adapter - reinforced tube - installed
    Dust brush adapter – reinforced tube – installed

    Now, let’s see how long that repair lasts …

    The OpenSCAD source code as a GitHub Gist:

    //——————-
    // eBay horsehair dusting brush
    // Hacked for 3/4" Schedule 40 PVC stiffening tube
    module DustBrush() {
    union() {
    translate([0,0,40.0])
    rotate([180,0,0])
    difference() {
    union() {
    cylinder(d1=EndStop[OD1],d2=31.8,h=10.0);
    translate([0,0,10.0 – Protrusion])
    cylinder(d1=32.0,d2=30.0,h=30.0 + Protrusion);
    }
    translate([0,0,-Protrusion])
    cylinder(d1=26.0,d2=24.0,h=100);
    translate([0,0,-Protrusion]) // 3/4 inch Sch 40 PVC
    PolyCyl(27.0,100);
    }
    translate([0,0,40.0 – Protrusion])
    MaleFitting();
    }
    }
  • Kitchen Chair Leg Glide

    A stick in the ground marking a repair:

    Kitchen chair leg glide
    Kitchen chair leg glide

    The white plastic glide / slide / foot / cap / whatever is molded around a simple nail that broke a divot out of the foot. Fortunately, I caught it before the nail gouged the kitchen floor.

    Under normal conditions, I’d replace the foot from my heap, but, my heap having become somewhat depleted, I swapped in another chair, chipped out the broken plastic, undercut the divot, filled it with JB Kwik epoxy, gooshed the foot in place, and taped it until it cured.

    We’ll see how long this lasts …

  • Hair Dryer Fuzz

    Mary reported that her hair dryer didn’t have nearly as much oomph as in the Good Old Days. After a struggle to remove the rear cover (with no affordance to turn in the direction required to release the hidden latches), this appeared:

    Hair dryer inlet fuzz
    Hair dryer inlet fuzz

    One snort from the shop vacuum returned it to the Good Old Days.

    That was easy…

  • Scale Cover Repair

    You can only drop a small kitchen scale so many times before the plastic cover / weighing tray breaks:

    Magnum scale cover - glued and clamped
    Magnum scale cover – glued and clamped

    The trick was to anchor the cover to the glass plate with the big clamp so that the smaller clamps could exert force straight down on the edge, without flipping the lid due to the bevel. With that all set up: apply IPS #4 to the broken edges, insert pieces, apply clamps, wait overnight.

    For the record, my morning mug o’ green tea starts with 4 (-0.0 +0.4) g of leaves…