Ed Nisley's Blog: Shop notes, electronics, firmware, machinery, 3D printing, laser cuttery, and curiosities. Contents: 100% human thinking, 0% AI slop.
One of the ribs in the six-passenger umbrella we keep in the van snagged on something and snapped its fitting on the spreader strut:
Umbrella strut – broken connector
This being wonderful engineering plastic that cannot be solvent-bonded, epoxy is the only adhesive that will work. However, those joints undergo tremendous stress in a deployed umbrella, so a bare epoxy joint won’t have enough strength for the job. What to do?
Wonder of wonders, when I got the umbrella into the Basement Laboratory Repair Wing, I discovered:
The not-quite-round strut fitting stub slipped right into a short brass tube from the heap and
Just enough of the fitting remained on the rib to anchor the tubing
A silicone tape wrap kept most of the epoxy inside while it cured:
Umbrella strut – epoxy curing
Clearing off a few blobs made it all good:
Umbrella strut – brass tubing splint
We don’t play golf, but such a big umbrella keeps most of the rain off two people; it’s a tchotchke from back when Mary worked at IBM (hence the color scheme). We call it our “six-passenger” umbrella because it looks about that big when we deploy it…
The absurdly heavy pump nozzle atop the kitchen sink soap dispenser seemed more wobbly than usual. Some investigation suggested the fitting atop the plastic pump has gotten smaller, which may be due to having the nozzle wobble around on it.
In any event, a wrap of Kapton tape snugged it up just fine:
Sink soap dispenser pump
We’ll see how long that lasts; this thing may be nearing the end of its useful life.
The slop sink in the rental house developed a drip and, unlike our kitchen faucet, required only a new washer. Of course, choosing the right size from that assortment posed a bit of a problem:
Slop sink valve with washers
The old washer is in the upper right; you can see the indentation from the valve seat.
There’s a variety of sizes & shapes; these represent just the closest matches. I have no idea what 3/8, 3/8R, and 3/8L might signify, but they’re all slightly different, some with conical cross-sections that may also be slightly different. Worst case, of course, you can sand down the rim of a too-large washer to make the diameter come out right.
The washer just in front of the old one has information molded right into the back: GOLDEN STATE 10¢ 1/2. Now there’s a show of confidence in price stability that you don’t see much any more!
I found one that fit snugly in the recess of the valve stem, turned the screw tight, and it’s all good.
Friends of ours planted a few dozen Liriope spicata as a border around their nicely trimmed flower garden. This did not work out well, as the stuff spreads like a weed and duplicated beyond their wildest imagination. However, this part of the description caught our attention:
No serious diseases or pests occur for creeping lilyturf. […] Lilyturf is reported to have little wildlife value.
Translation: nothing kills the stuff and deer don’t eat it. Sounds like exactly what we need for the section of the front yard that slopes down to the road, where mowing poses a threat to life & limb.
We said we’d take it, they dug it out and bagged it, I hitched up the bike trailer, and we paid them a visit:
YAK Bike Trailer – 55 lb of grass
They’re a few miles off the south end of the Dutchess Rail Trail, which is (by definition) pretty much dead flat and made the trip a lot easier: that load of grass added up to 55 pounds! They dropped off a few bags on their next trip past our house, which tells you how much they wanted to get rid of it.
I wielded the post-hole digger to prepare about 100 sites, shook the dirt off the existing grass roots to backfill the holes, we divided the new clumps by chopping them with a shovel, and a day later we had everything installed and watered down:
The handle cracked and fell off this ball valve while I collected the hoses and suchlike from the Vassar Farms plot:
Ball valve with broken handle
Surprisingly, it’s not plastic, but (most likely) some cheap & grainy pot metal that wasn’t designed for durability. Rather than throw out that nice brass and stainless steel valve body, I figured a new handle was in order.
To the Basement Laboratory Machine Shop Wing!
The ball rotates freely inside the valve with the handle missing, so I found an aluminum rod (which, IIRC, was the original kickstand from my Linear Mach III ‘bent) that exactly fit the ball opening’s ID:
Ball valve – removing nut
What with it being a dark and stormy night outside (and having shut down all the computers in anticipation of a monster thunderstorm), I decided to get medieval with some hand tools. The first step involved finding an aluminum plate of about the right size and thickness, with markings left over from whatever I’d been building when it last saw the ceiling lights:
Ball valve handle – initial layout
After carefully drilling & filing the shaft hole, it looked like it’d work fine. Then I realized that, for whatever reason, the original design aligned the handle parallel to the hose when the valve was closed, which made very little sense when analyzed according to the Principle of Least Surprise.
So I drilled-and-filed another hole on the other end at right angles to the first one:
Ball valve handle – proper alignment
The original handle had two bumps molded on the bottom that acted as stops at each end of its 90° rotation. I figured a pair of 10-32 screws would suffice, not to mention they’d provide a bit of adjustment in case I blundered the hole positions. I planned to chop these stubs to whatever set the proper length below the plate:
Ball valve handle – trial fit
It turned out that the proper length was just about exactly that of a 1/4 inch 10-32 set screw flush with the top of the plate, so that’s what I used instead. They’re located one radius out from the outline of the valve body; trace the body shape on the handle in each orientation, eyeball one setscrew radius out from those intersections, and drill the holes.
Lay out a nice handle shape by eye, rough it on the bandsaw, introduce it to Mr Belt Sander for final shaping, touch up the concave corners with a rat-tail file, scuff the flat surfaces clean with a Dremel stainless steel wire brush to produce a used-car finish (nice polish over deep scratches), and it’s all good:
Ball valve handle – top view
The knob on the end is actually a foot intended for the bottom of a widget case:
Ball valve handle – bottom view
It won’t get leak-tested until next year, but what could possibly go wrong?
One thing, perhaps: that screw likely lies too close to the hose, particularly one sporting a replacement connector. I may be forced to bend the narrow part of the handle up a bit…
And here’s the name-brand towel for a mere one cent more per hundred towels:
Bounty Select-a-Size Towel – unit price
How can this be?
Easy! Notice that the name-brand towel allows you to tear off a smaller sheet, which is actually a good idea. Even better, at least from their perspective: more sheets per package = lower unit price! I didn’t check the actual mini-towel size, but surely it’s less than half the usual size, so the comparable unit prices is more than a factor of two higher than shown.
I suppose it’s only a matter of time before WalMart slices their towels in half to get an even better unit price.
Carpet and floor tile used to be priced per square yard. Now it’s roughly the same dollar amount per square foot.
The Nike cycling shoes I bought some years ago (at a steep discount when they got out of the cycling shoe biz) close with a ratcheting plastic strap rather than laces, so I bought a spare set of straps: the plastic part always breaks first. As it turned out, a coil spring inside each latch failed and the stub end (on the right side here) gradually worked its way between the latch tab and the frame:
Cycling shoe latch – broken spring
Eventually this got to the point where the latches jammed and I had to do something. The first step was to drill out the rivet holding the spring and tab in place:
Drilling latch rivet – magnetized bit
You’ll note the rich collection of swarf clinging to the drill bit, which indicates this one hasn’t been used since a lightning strike magnetized all the steel in the house. A pass through that demagnetizer shook off the swarf and prepared the bit for the next time.
Releasing all the parts shows the problem:
Nike cycling shoe latch – broken spring
The OEM springs used 24 mil spring wire that, surprisingly, matched a box of music wire in the Basement Laboratory Warehouse Wing. The spring coils have 5 turns that just clear the 3 mm rivet that I recycled as a mandrel; I think a 2.5 mm pin would produce a better fit. Not being a fan of rivets, I replaced them with 4-40 machine screws, even though the threads probably won’t do the aluminum frame any good at all.
A protracted bending and wrapping session produced a reasonable approximation of the OEM spring:
Latch spring – formed
It’s worth noting that each of those coils uses up about 55 mm of wire: 5 × 3.5 mm × π. Cut an excessively long piece from the music wire coil!
Trimming and shaping the ends to fit through the notches and around the outside of the frame shows that my wire-bending skills need considerably more practice. This spring (the second one I made) also shows that my beginner’s luck with the first coils wore off all too quickly:
OEM springs with homebrew replacement
But both springs fit and work fine, so I’ll call it done for now:
Repaired latch – nut side
Will a replacement spring break before the plastic strap?