The Smell of Molten Projects in the Morning

Ed Nisley's Blog: Shop notes, electronics, firmware, machinery, 3D printing, laser cuttery, and curiosities. Contents: 100% human thinking, 0% AI slop.

Tag: Repairs

If it used to work, it can work again

  • Epson R380 Printhead Clog: Syringe Flush

    The saga of the blocked magenta printhead on my Epson R380 continues. The inlet posts that tap the R380 printer’s ink cartridges…

    R380 printhead ink inlets
    R380 printhead ink inlets

    … look like they ought to fit some sort of tubing and, indeed, a bit of rummaging produced a hank of suitable thick-walled plastic stuff. Heating one end until it went clear and floppy, then jamming it over a syringe’s Luer fitting produced a workable flushing tool:

    Syringe with tubing to fit R380
    Syringe with tubing to fit R380

    I folded a tissue, laid it over the sponges and wipers at the printhead park position, then pushed the ink tank carrier over the tissue to absorb the spray. Squirting three syringes full of 10% ethanol through the head cleaned out a few of the blocked jets, but didn’t produce a complete fix.

    Next up: homebrew window cleaner, diluted about 1:3 to knock back the ammonia concentration.

  • Canon SX230HS Lens Cap: Regluing

    I dropped that lens cap and the sheet-metal disk popped out; evidently the acrylic caulk doesn’t really count as an adhesive. Cleaned out the residue, ran a thin layer of urethane adhesive around the rim, and applied some clamps:

    Re-clamping the cover
    Re-clamping the cover

    Cleaned out the inevitable urethane bubbles that emerge from even the most minute opening and it’s all good.

  • Epson R380 Printhead Clog: Teardown Failure

    So the Epson R380’s magenta printhead has clogged and cleaning it doesn’t have any effect. I figured I’d pop the printhead out, rinse off the crud, and see if that improved the situation. Turns out, you can’t get there from here…

    The first step is removing the printer side panels, which involves sliding a steel strip into the not-really-vent slots along the side to release the catches as described there. This picture shows what’s going on inside:

    R380 side panel locking tab release
    R380 side panel locking tab release

    You must hit that slot in the catch with the strip, so the strip must be no wider than 15 mm = 5/8 inch and tapering the end would certainly help. After I removed the panels, I broke those latch tabs off; the panel has locating tabs that align the edges, so the latch tabs just keep you out.

    In any rational printer, accessing the printhead for cleaning would be trivially easy. Epson has a different attitude: KEEP OUT!

    My original idea was to release the rod upon which the ink tank carrier slides, then pull the whole thing out, but it turns out the rod is also a shaft that transmits rotary motion from one side of the printer to the other, plus a mechanism to raise and lower the printhead over the cleaning station (and, perhaps, the DVD carrier that I’ve never used). A vast assortment of gears, clips, encoder wheels, and doodads affixed to each end convinced me not to go that route right now.

    The left side includes an impossibly delicate rotary encoder disk blocking the end of the shaft:

    R380 left side mechanism
    R380 left side mechanism

    Prying the spring out of the shaft notch allows it to slide to the right until another spring clip slams up against the inside of the frame on the right side. That clip may be pry-able, but it’s carefully arranged so as to be maximally inconvenient to reach.

    R380 right side interior
    R380 right side interior

    The ring holding the gear in place must be removable, somehow or another, even without an obvious hole or tab:

    R380 right side mechanism
    R380 right side mechanism

    With that encoder wheel blocking the left end of the rod, I gave up.

    Then I tried to dismantle enough of the ink tank carrier to release the printhead. The first step removed the tank carrier’s two side panels, both of which use pull-out clips to prevent them from sliding. A view of the removed panels shows the tabs:

    R380 Ink Tank Carrier side panels latches
    R380 Ink Tank Carrier side panels latches

    The outside panel requires jamming a small screwdriver behind that tab at an awkward angle, then the panel slides downward:

    R380 Ink Tank Carrier - right side cover
    R380 Ink Tank Carrier – right side cover

    You can release the inside panel with a fingernail near the top of the (unmarked, but obvious) tab outlined in white on the far right side, then slide upward:

    R380 Ink Tank carrier - interior
    R380 Ink Tank carrier – interior

    The magenta circles mark three screws that secure the printhead plate to the carrier, but it won’t do you any good. The two rear screws require a narrow-shaft Philips #1 driver and you cannot get the screws out through the holes; I managed to get them back in place, but don’t loosen them until you figure out how to remove the assembly holding the electrical contacts for the ink tanks.

    That assembly, marked by the six color panels, slides vertically into the rear wall of the carrier and seems to have a latch on the rear wall of the tank carrier. Of course, you can’t access the latch without dismantling the damn printer.

    So I put everything back together again and the printer works no worse than it did before. I’m considering connecting a syringe with length of tubing to the magenta inlet port, then forcing a toxic mix of water, alcohol, and detergent through the printhead:

    R380 printhead ink inlets
    R380 printhead ink inlets

    Given that the printer cost something like $15 after rebate, it’s pretty much fully depreciated by now…

  • HelloDirect Headset Switch Cleanout

    The headset / phone switch in my ancient HelloDirect phone headset became increasingly intermittent and finally stopped switching at all, so I tore the thing apart. It has two snap latches on each side in addition to the single screw in the bottom:

    HelloDirect headset interface - top interior
    HelloDirect headset interface – top interior

    The 4PDT switch just to this side of the volume drum can’t be taken off the board without unsoldering all 12 terminals and two case anchors, so I just eased some DeOxit Red into the openings and vigorously exercised it. That seems to have done the trick.

    I cleaned out a bunch of fuzz and a spider husk while the hood was up…

     

  • BOB Yak Trailer: Replacement Pin Straps

    My old BOB Yak trailer mounts to the bike axle with stainless steel grenade pins, which works fine. After all these years, alas, the rubber straps securing the pins to the frame have rotted away. The original straps are nicely molded affairs:

    BOB Yak - original pin strap
    BOB Yak – original pin strap

    I snipped a large O-ring, deployed four small cable ties, and this ought to last for another decade:

    BOB Yak - new pin strap
    BOB Yak – new pin strap

    The strap in the first picture hadn’t quite broken, but the rubber was cracked and ready to snap. So I made a preemptive strike…

    And, yes, one can buy replacement pins and straps, but where’s the fun in that?

  • KitchenAid Mixer Pivot Shaft Tweak

    The shaft that tilts the mixer head has started walking sideways out of its hole, which is not to be tolerated. Looking up inside the base column shows a locking screw that’s worked loose:

    KitchenAid mixer - pivot shaft and locking screw
    KitchenAid mixer – pivot shaft and locking screw

    I took the thing apart and filed a flat on the shaft:

    KitchenAid mixer pivot shaft - added flat
    KitchenAid mixer pivot shaft – added flat

    And then a dab of Loctite on the screw will prevent that from happening again:

    KitchenAid mixer pivot locking screw
    KitchenAid mixer pivot locking screw

    It’s still piddling oil on the countertop. If you have one of these things, always store it with the head tilted upward. That makes the oil run down the column onto the counter, rather than through the planetary gears into the mixing bowl…

     

  • Soldering Third Hand Alligator Clip Improvement

    The third hand grabbers I have all put bare alligator clip ferrules in the adjustable sockets with a thumbscrew to secure them. Over time, that thumbscrew crunches the ferrule and makes the clip hard to adjust. This has become enough of an annoyance that I rummaged around in the brass tubing cutoffs to find some that fit into the ferrules:

    Alligator clip with brass tube insert
    Alligator clip with brass tube insert

    Given the sorry state of the ferrules, they required quite a bit of squeezing and shaping until that tube fit inside, but after that they rounded up nicely.

    I suppose I should solder the tubes in place, but …