Ed Nisley's Blog: Shop notes, electronics, firmware, machinery, 3D printing, laser cuttery, and curiosities. Contents: 100% human thinking, 0% AI slop.
Tag: Improvements
Making the world a better place, one piece at a time
With the quilt off the HQ Sixteen, I could install the 24 V power supply for the Nose Ring Lights:
HQ Sixteen Nose Ring Lights – power supply installed
IMO, black nylon screws look spiffier than brass.
The solid model shows the covers have a 2 mm overlap with the power supply case to keep them lined up:
HQ Sixteen Nose Ring Lights – power supply cover – solid model
I managed to reuse three of the five holes from the previous 12 V power supply and drill only three more:
HQ Sixteen Nose Ring Lights – power supply detail
The tops of the power supply ears aren’t quite flat, giving the standoffs a slight tilt that the covers mostly drag back into alignment.
The M4 brass standoffs screw into holes tapped in the thick plastic, thus eliminating nuts inside the power pod:
HQ Sixteen Nose Ring Lights – power supply wiring
The yellow silicone tape wraps two pairs of Wago connectors that dramatically simplify electrical connections in anything with enough space for their chonky bodies.
In the unlikely event you need such things, the original post links the OpenSCAD source code.
With the power supply in place, I think I can put some LED strips under the arm of the machine to light up more of the quilt than the nose lights can reach. More pondering is in order.
A critter made off with our battered plastic rain gauge, so I set up an Ambient Weather WS-5000 station to tell Mary how much rain her garden was getting. I added the Official Bird Spike Ring around the rain gauge to keep birds off, but robins began perching atop the anemometer while surveying the yard and crapping on the insolation photocell.
After a few false starts, the anemometer now has its own spikes:
Weather station with additional spikes
It’s a snugly fitting TPU ring:
Weather Station Spikes – build test piece
The spikes are Chromel A themocouple wire, because a spool of the stuff didn’t scamper out of the way when I opened the Big Box o’ Specialty Wire. As you can tell from the picture, it’s very stiff (which is good for spikes) and hard to straighten (which is bad for looking cool).
The shape in the middle is a hole diameter test piece. Next time around, I’ll use thicker 14 AWG copper wire:
Weather station spikes – test piece
The test piece showed I lack good control over the TPU extrusion parameters on the Makergear M2, as holes smaller than about 2 mm vanish, even though the block’s outside dimensions are spot on. This application wasn’t too critical, so I sharpened the wire ends and stabbed them into the middle of the perimeter threads encircling the hole.
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It just barely clears the curved air guide inside:
PolyDryer airlock plate – tiny fan installed
The tea bags full of desiccant allow some wind between them and the filament in the spool, but I obviously must re-think that setup. There’s enough clearance for what should be reasonable circulation, so i defined it to be good enough for now.
The box of TPU started at 25 %RH, dropped to 22 %RH overnight, then returned to 25 %RH the next day:
PolyDryer TPU – 25 pct RH
Now that I’m watching more often, I’ve seen the meter glitch to 10% for a few seconds:
PolyDryer TPU – 10 pct RH glitch
A humidity indicator card suggests the air is under 20 %RH:
PolyDryer TPU – humidity indicator card
It may be the filament can outgas water vapor as rapidly as the desiccant can remove it, but I expected the fan to make at least a little difference.
The new shower head’s hose dangled directly in front of the faucet knob, so I conjured a simple clamp to pull the down-going half over to the side of the stall and keep the up-going half away from the faucet:
Shower head hose clamp – installed
The black nylon M6 screw goes into a hole tapped in the plastic cap atop the aluminum extrusion; I was mildly surprised that worked as well as I hoped. It’s basically invisible from outside the shower stall.
Stipulated: laser-cut 3 mm acrylic probably isn’t the right material for the job, but it’s a quick & easy way to discover if that’s the right place to clamp the hose.
While installing those two pieces, it occurred to me the result would be much stronger if the two “jaws” overlapped and had a pair of screws holding them together, so the LightBurn layout includes that idea for the next time:
Shower Head Hose Clamp – LightBurn layout
The Hole Template simplified getting the hole dead center in the plastic cap, because drilling it required an awkward reach across the end of the vanity.
There is zero chance this will fit your shower & hose, but now you have the general idea.
The Basement Shop has 50±5% relative humidity, with the top held down by a hulking dehumidifier (plus a box fan stirring the air) and the bottom supported by being a basement. As a result, the 3D printer filament stabilized at about 50% RH, which seemed to work well enough for PETG.
That’s activated alumina desiccant, mostly because it’s reputed to have more capacity and a lower ultimate humidity than silica gel, but it likely doesn’t make much difference.
In addition to 25 g of desiccant in the PolyDryer meter case, I dropped five teabags holding 10 g each in the bottom of the box for more capacity. I measure the desiccant by putting 75.0 g into a cup, putting 25.0 g in the PolyDryer meter box (aided by a Polydryer Desiccant Funnel), 10.0 g into four teabags, and whatever’s left into the fifth teabag, thus eliminating rounding errors in the smaller quantities.
The stabilized humidity inside the boxes seems to depend on the amount of filament on the spool:
Nearly full → 25% to 30% RH
Half full → 20%-ish RH
Nearly empty → 10% to 15% RH
I think the humidity level comes from the filament outgassing water vapor through its (limited) surface area on the outer layer around the spool. The difference between that rate and the desiccant’s ability to remove water vapor from the (unmoving) air in the box sets the stable humidity: more surface area → more water vapor → higher humidity.
After the filament eventually dries out, the humidity should decrease, but diffusion is a slow process. More likely, the humidity will remain stable as the printer pulls filament from the outer layer and exposes the somewhat wetter plastic within.
The heater and fan inside the PolyDryer base unit circulates hot air through the box around the spool, but depends on the desiccant to remove water vapor. Running the base unit for 6 or 12 hours makes little difference in the stabilized humidity, so I think the desiccant is doing the best it can as the filament outgasses more water vapor.
Using Air Exchanger vents seems to make no difference, likely because the desiccant must then pull more water vapor out of the incoming 50% RH basement air. A psychrometric chart says 50% RH air at 60 °F becomes 10% RH air at 120 °F, but moisture in the filament wrapped around the spool can’t escape any faster.
So, for example, a full spool of TPU starting at 25% RH:
PolyDryer humidity – TPU start
Six hours of drying pulls it down to 22%:
PolyDryer humidity – TPU finish
After sitting overnight it’s back at 25%:
PolyDryer humidity – TPU after 14 hr
Admittedly, that was with the vents in place, but the closed box started at 25% RH after sitting around for a week or so following a similar drying cycle.
The desiccant had absorbed 4 g of water since I put it in, so it hasn’t been entirely idle.
Which suggests 75 g of activated alumina desiccant is workin’ hard and doin’ swell in there, with the filament acting as an essentially infinite reservoir of water vapor.
I haven’t noticed any particular difference in PETG print quality and the TPU hasn’t gotten enough mileage to notice much trouble, but reducing the MMU3 buffer clutter was totally worth the effort.
We don’t know what the proper term might be for this part of the machine, but it looks sorta like a nose and the lights form most of a ring around it, so I’m going with “Nose Ring Lights”:
Handi-Quilter sells a ring light for machines manufactured a decade later than ours, but it uses a built-in USB jack this machine lacks.
One of two (apparently) unused M4 holes on the left side of the machine frame suggested a mounting point for a 3D printed bracket:
HQ Sixteen Nose Ring Lights – solid model
The ramp matches the 3° (-ish) mold draft of the machine frame, which I initially ignored by angling the tab, but a tilted frame looked awful; it’s now aligned with local horizontal..
A few iterations got all the pieces & holes in their proper places:
HQ Sixteen Nose Ring lights – iterations
The smaller (rampless) bracket has three LED strips, but a quick test showed more light would be better:
HQ Sixteen Nose Ring lights – bottom view
The lack of a transparent-ish cover is obviously unsuitable for a commercial product, but the key design goal is to not interfere with spreading as much light as possible across as much of the quilt as possible. The black JB Weld Plastic Bonder blobs keep the 24 VDC supply out of harm’s way, which is as good as it needs to be for now.
The bracket has three sides, because the right side of the machine has all the thread guide hardware. Putting anything over there seemed likely to interfere with either thread movement or fingers making adjustments.
Fortunately, the wider bracket doesn’t stick out too far beyond the machine frame and the doubled LED strips create a much smoother light pool:
HQ Sixteen Nose Ring lights – left front view
Yes, the quilt is focused and the LED frame is blurred.
The larger light-emitting area reduces the shadow under the left rod (supporting the ruler foot) enough to be unobjectionable.
A 0.2 mm layer thickness transforms the smooth ramp into stair steps:
HQ Sixteen Nose Ring Lights – PrusaSlicer
They’re inconspicuous after the bracket is installed.
The Chin Light ran on 12 V and these strips require 24 V, so the OpenSCAD code creates a pair of endcaps for the new supply, which is of course completely different than the old supply. Setting that up must await quilt completion.
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For reasons not relevant here, Mary is completing a friend’s quilt for the family. Part of the existing design involves stitching arcs around each side of a myriad small blocks across the quilt:
Small arc quilting ruler – block border
After free-motion quilting a few blocks, Mary decided the peak of the curve looked good at ⅜ inch from the block edge. This sort of thing is generally done by “ruler quilting” with the machine’s foot guided by a ruler, but none of her considerable assortment of quilting rulers had exactly the arc required for that curve.
Knowing the blocks are 2-¼ inch on a side and the arc is ⅜ inch tall, the Chord Equation gives the 1-⅞ inch radius of the circle matching the arc. Using proper terminology:
With those numbers in hand, producing a suitable quilting ruler is straightforward:
Judy Quilt – small arcs – LightBurn layout
The legends are backwards, because the lines must be engraved on the bottom of the ruler to eliminate parallax through the ¼ inch acrylic sheet:
Small arc quilting ruler – alignment
She can now eyeballometrically align the engraved square with the edges of the block to put the curved edge at the right place to guide the foot:
Small arc quilting ruler – stitch line
After half a dozen blocks, she reports the ruler works as intended and the duplicated Start / Stop buttons on the improved hand grips let her control the machine with either thumb. She uses Stitch Regulator mode to produce a uniform line of stitches regardless of speed variations around the arc.
Now she can finish the quilt and have all those curves look the way she wants.