The Smell of Molten Projects in the Morning

Ed Nisley's Blog: Shop notes, electronics, firmware, machinery, 3D printing, laser cuttery, and curiosities. Contents: 100% human thinking, 0% AI slop.

Author: Ed

  • USB Charger: Safety FAIL

    USB Charger: Safety FAIL

    Mary reported a problem unplugging the USB charger powering the light pad (the successor to the pad I repaired) she uses for quilting layouts:

    USB Charger - as found
    USB Charger – as found

    Yes, that blade is sticking out of the hot (“Line”) side of the outlet.

    The only way into the charger was through its other end:

    USB charger - interior top
    USB charger – interior top

    Because I had no intention of returning it to service, I tried pushing the errant blade back in place, only to have it overshoot the mark and bulldoze various parts aside:

    USB charger - PCB blade contacts
    USB charger – PCB blade contacts

    The two upright shapes contact the blades, but do not lock them in place. The PCB pulled easily out of the case, with no objection from the remaining (“Neutral”) blade.

    The blades are simple steel bars press-fit into the plastic case, without holes / dimples / notches to lock them into the plastic. As far as I could tell, they were not molded in place.

    I tossed the corpse into the e-waste box, extracted another USB charger from the Box o’ USB Chargers and returned the light pad to service.

    I do have a few Genuine UL Listed USB chargers, but these are not among them.

  • Fitbit Charge 5 Charging Stand

    Fitbit Charge 5 Charging Stand

    My Fitbit Charge 5 has become fussy about its exact position while snapped to its magnetic charger, so I thought elevating it above the usual clutter might improve its disposition:

    FitBit Charge 5 stand - installed
    FitBit Charge 5 stand – installed

    The Charge 5 now snaps firmly onto its charger, the two power pins make solid contact, and it charges just like it used to.

    The solid model comes from Printables, modified to have a neodymium ring magnet screwed into its base:

    Fitbit Charge 5 stand - solid model section
    Fitbit Charge 5 stand – solid model section

    Which looks about like you’d expect;

    FitBit Charge 5 stand - added magnet
    FitBit Charge 5 stand – added magnet

    A layer of cork covers the bottom and it sits neatly atop the USB charger.

    The OpenSCAD source code punches the recesses and produces the bottom outline so LightBurn can cut the cork:

    // FitBit Charge 5 Stand - base magnet
    // Ed Nisley - KE4ZNU
    // 2025-09-05
    
    include <BOSL2/std.scad>
    
    Layout = "Build";       // [Build, Base, Section]
    
    module Stand() {
      difference() {
        left(38/2) back(65/2)
          import("Fitbit Charge 5 Stand.stl",convexity=10);
    
          down(0.05)
            cylinder(d=12.5,h=5.05,$fn=12);
          up(5.2)
            cylinder(d=3.0,h=10.0,$fn=6);
      }
    }
    
    //-----
    // Build things
    
    if (Layout == "Build")
      Stand();
    
    if (Layout == "Base")
      projection(cut = false)
        Stand();
    
    if (Layout == "Section")
      difference() {
        Stand();
        down(0.05) fwd(50)
          cube(100,center=false);
    }
    
    

  • All’s Well Who Ends Well

    All’s Well Who Ends Well

    Eventually this happened:

    Negative COVID tests
    Negative COVID tests

    Three weeks, more or less, from my exposure to clearing the hurdle. Mary, being tougher than I, got it done in two.

    For the better part of the first two weeks I was in bed ten hours every night, plus an hour or two of afternoon nap (no milk & cookies, drat), plus dragging around the house getting nothing done.

    No major health problems, good blood oxygen levels throughout, no loss of smell apart from what you’d expect during three days of complete nasal blockage, and we’re both feeling OK-ish now.

    However, we are making more than the usual number of stupid mistakes, which is one way we know we’re not really OK yet.

    Back to the Basement Shop, with considerable caution …

    Memo to Self: That was the first time in four years you didn’t wear a mask in close quarters. Don’t ever do that again.

  • Dances With Disease

    Dances With Disease

    So then this happened:

    Positive COVID test
    Positive COVID test

    This being my first round in this particular rodeo, I’m unlikely to be doing anything useful for a week or two.

    Paxlovid incoming …

    Protip: Wear your mask, no matter how much trouble other folks have understanding your accent.

  • Makergear M2: Repositioned Filament Drive Gear

    Makergear M2: Repositioned Filament Drive Gear

    AFAICT, the Makergear M2’s filament drive gear has been in the same place on the motor shaft since I set it up nearly five years ago:

    Makergear M2 - original filament drive pulley position
    Makergear M2 – original filament drive pulley position

    The filament rides along the white trail close to the front of the gear. This worked fine with PETG, but TPU occasionally squeezed out through the small gap toward the front of the extruder, so I moved the gear a few millimeters forward:

    Makergear M2 - improved filament drive pulley position
    Makergear M2 – improved filament drive pulley position

    The track on the idler bearing shows the filament is neatly centered where it should be:

    Makergear M2 - filament idler bearing position
    Makergear M2 – filament idler bearing position

    I haven’t adjusted the spring pressure on the idler, but it’s probably too high for TPU. If it continues to work, I’ll continue to do nothing.

  • Makergear M2: BuildTak Platform Alignment

    Makergear M2: BuildTak Platform Alignment

    The Z-axis switch on the Makergear M2 put Z=0 on the surface of the BuildTak platform and a quick leveling got the TerraCycle tires printed, but a more thorough alignment seemed in order.

    I wanted to align the magnetic base plate first, but it has a lot of magnets and steel tools just weren’t going to work:

    MakerGear M2 BuildTak - FlexPlate magnets
    MakerGear M2 BuildTak – FlexPlate magnets

    So I put the BuildTak FlexPlate on top and deployed the taper gauge, with all the magnetic fields held safely inside the steel sheet below the surface:

    MakerGear M2 BuildTak - taper gauge
    MakerGear M2 BuildTak – taper gauge

    The plate turned out to be mostly flat, with two high spots at the center front and back. A few strips / layers of Kapton tape raised the lowest spots along the sides and middle enough to get the whole surface Close Enough™:

    MakerGear M2 BuildTak - FlexPlate shims
    MakerGear M2 BuildTak – FlexPlate shims

    That’s really thick 4 mil = 0.1 mm tape, not puny 1 mil stuff. Two layers added enough height to very slightly warp the steel plate when held down by all those magnets.

    The final result was flat within ±0.05 mm across the entire plate, with those two high spots reduced to +0.2 mm.

    At which point, an array of thinwall calibration boxes came out perfectly:

    MakerGear M2 BuildTak - test square layout
    MakerGear M2 BuildTak – test square layout

    The high spots lie outside the skirt at the front & rear of the plate, where they should be easy to avoid with most models I can imagine building in TPU. Stipulated: I have a stunted imagination.

    TPU boxes are bendy little things with 0.45 mm walls:

    MakerGear M2 BuildTak - test square
    MakerGear M2 BuildTak – test square

    After I got the plate flattened, even a single-thread wall of TPU sticks to BuildTak like it was glued there.

    I had PrusaSlicer print them sequentially to avoid excessive back-and-forth, although combining 2 mm Retraction with Avoid crossing perimeters has eliminated much of the previous stringing:

    Terracycle Chain Idler Tire - TPU stringing
    Terracycle Chain Idler Tire – TPU stringing

    I modified the startup G-Code to purge & wipe the nozzle at the right-front corner of the plate:

    MakerGear M2 BuildTak - nozzle cleaning
    MakerGear M2 BuildTak – nozzle cleaning

    If I’d done that at the start, the BuildTak surface wouldn’t have a small divot melted into the center front edge where the previous G-Code paused the nozzle at the edge of the glass plate while heating. Pausing a millimeter off the diagonal seems to isolate the hot nozzle from the plastic surface.

    The revised startup G-Code, with the earlier clearing motions commented out:

    ;-- PrusaSlicer Start G-Code for M2 starts --
    ; Ed Nisley KE4NZU
    ; Makergear V4 hot end
    ; Origin at platform center, set by MANUAL_X_HOME_POS compiled constants
    ; Z-min switch at platform, must move nozzle to X=135 to clear
    ; 2025-08-29 tweak priming spot to avoid scorching BuildTak surface
    G90                                      ; absolute coordinates
    G21                                      ; millimeters
    M83                                      ; relative extrusion distance
    M104 S[first_layer_temperature]          ; start extruder heating
    M140 S[first_layer_bed_temperature]           ; start bed heating
    M17                                      ; enable steppers
    G4 P500                                  ; ... wait for power up
    G92 Z0                        ; set Z to zero, wherever it might be now
    G0 Z10 F1000                  ; move platform downward to clear nozzle; may crash at bottom
    G28 Y                         ; home Y to clear plate, offset from compiled constant
    G28 X                         ; home X, offset from M206 X, offset from compiled constant
    G0 X135 Y0 F15000             ; move off platform to right side, center Y
    G28 Z                         ; home Z to platform switch, offset from M206 Z measured
    G0 Z2.0 F1000                 ; get air under switch
    ;G0 Y-126 F10000               ; set up for priming, zig around corner
    ;G0 X0                         ; center X
    ;G0 Y-125.5                    ; just over platform edge
    G0 Y-121 F15000               ; set up for priming
    G0 X96                        ; diagonally beyond trimmed corner of BuildTak plate
    G0 Z0 F500                    ; exactly at platform
    M190 S[first_layer_bed_temperature]   ; wait for bed to finish heating
    M109 S[first_layer_temperature]       ; set extruder temperature and wait
    G1 E25 F200                           ; prime to get pressure, generate blob on edge
    ;G0 Y-123 F5000          ; shear off blob
    ;G0 X15 F15000           ; jerk away from blob, move over surface
    ;G4 P500                 ; pause to attach
    ;G1 X45 F500             ; slowly smear snot to clear nozzle
    G0 X94 Y-119 F5000      ; shear off blob
    G0 X90 F15000           ; jerk away
    G4 P500                 ; pause
    G1 X50 Y-124 F500       ; smear snot
    G1 Z1.0 F2000           ; clear bed for travel
    ;-- PrusaSlicer Start G-Code ends --
    
    

    With all that done, the Small Hole Gauge came out much better:

    Makergear M2 BuildTak - small holes - front
    Makergear M2 BuildTak – small holes – front

    The one on the left came from the M2’s glass plate (with a brim barely improving its adhesion) and the one on the right was on BuildTak after all the fussing; I just noticed I laid them out in opposite directions.

    An edge view shows the fuzzy surface on the left:

    Makergear M2 BuildTak - small holes - edge
    Makergear M2 BuildTak – small holes – edge

    The tiniest holes in both are undersized, but AFAICT you could ram a screw through that bendy sheet without much effort.

    The BuildTak sheet works well enough that I have not tried the PEI-covered FlexPlate, which I’m sure will require similar shimming to get a level surface.

    And, no, I am not going to install a surface probe on the M2’s hot end.

  • Terracycle Chain Idler Tires: TPU Tweakage

    Terracycle Chain Idler Tires: TPU Tweakage

    Although the 3D printed tires for our Terracycle chain idlers fit nicely, adjacent TPU threads didn’t bond well:

    Terracycle Chain Idler Tire - delamination
    Terracycle Chain Idler Tire – delamination

    Based on some earlier items, I’d been printing TPU at 220 °C, but 230 °C fuses the threads together:

    Terracycle Chain Idler Tire - correct settings
    Terracycle Chain Idler Tire – correct settings

    The filament turned out to be 1.79 mm diameter, rather than the nominal 1.75 mm, and a few iterations showed a 0.95 Extrusion Multiplier worked much better.

    Those were printed at 30 mm/s with 0.25 mm layer height.

    I now have a good stock of spare tires, each slightly different than all the others:

    Terracycle Chain Idler Tire - spares
    Terracycle Chain Idler Tire – spares

    The first two slightly delaminated printed tires will remain in service until they show signs of falling apart, because I’d rather ride the bike than fiddle with it.