The Smell of Molten Projects in the Morning

Ed Nisley's Blog: Shop notes, electronics, firmware, machinery, 3D printing, laser cuttery, and curiosities. Contents: 100% human thinking, 0% AI slop.

Category: Machine Shop

Mechanical widgetry

  • Silicone Handle Wrap

    Silicone Handle Wrap

    The common fate of all “soft touch” silicone handles is to become sticky and gooey. While some goo may be removable, I’ve found that wrapping self-bonding silicone tape around the mess both encapsulates it and maintains the grippiness of the original silicone.

    The most recent casualty is the decade-old ceramic crysknife I returned to service while the rest of the knives were being sharpened:

    Ceramic knife - silicone handle wrap
    Ceramic knife – silicone handle wrap

    While I was at it, I added griptivity to the leaf blower handle:

    Leaf blower - silicone handle wrap
    Leaf blower – silicone handle wrap

    Long years ago, before getting transparent silicone tape, I’d wrapped a kitchen slotted spoon:

    Kitchen spoon - silicone handle wrap
    Kitchen spoon – silicone handle wrap

    Stipulated: Butt-ugly and built to stay that way.

    Oddly, the handle on the matching spatula / scraper remains non-gooey to this day.

    Should you care more about form than function, this repair is not the one you seek …

  • Prusa MK4+MMU3 vs. Spool Join: Whoopsie

    Prusa MK4+MMU3 vs. Spool Join: Whoopsie

    Because nobody will ever see the Radiator Sleds, I started a batch with the tail end of the white PETG spool and set up the Spool Join function to switch to the retina-burn orange PETG when the white filament ran out.

    The two colors combined nicely on that layer:

    Prusa MK4 MMU filament joining
    Prusa MK4 MMU filament joining

    Unfortunately, the Spool Join didn’t work out quite right and I had to extricate the white filament from the MMU3, then coerce the orange filament into position.

    The key section of the MMU3 looks like this:

    Prusa MK4 MMU filament joiningPrusa Mk4 MMU3 selector
    Prusa MK4 MMU filament joiningPrusa Mk4 MMU3 selector

    The Selector assembly rides on the smooth rods, driven by the stepper motor on the far end of the leadscrew. It stops at one of the five filament tubes (visible to the left of the upper smooth rod, with filament tips showing), whereupon a drive gear pushes the filament into the Selector, under the FINDA sensor (the threaded fitting sticking out of the top), into the PTFE tube, down to the Nextruder, through the idler to trip the Filament Sensor, then into the extruder’s planetary drive gear.

    I think this happened:

    • The rear end of the white filament passed through the FINDA sensor
    • The MK4 reversed the Nextruder to drive the filament back into the MMU3
    • The rear end of the filament didn’t reenter its filament tube and escaped out to the side
    • The MMU3 drive gear couldn’t pull the filament backward, because the back end was misplaced
    • The Extruder planetary drive gear couldn’t pull the filament forward, because the front end was now above the gear
    • Both the FINDA and the Filament Sensor showed the filament was present, so the MK4 knew something was wrong

    Fortunately, I was watching the whole operation and could intervene.

    The MMU3 works well when the filament behaves properly, but it’s very sensitive to bends in the filament and misshapen ends. In this case, the white filament had the usual tight curve due to being would around the spool hub, which was enough to mis-align its end with the MMU3 tube while backing out.

    Trust, but verify.

  • Handlebar Grip Sleeve

    Handlebar Grip Sleeve

    Mary’s zero-mph crash loosened the starboard handlebar plug enough to let it eventually decamp for parts unknown. Its replacement, a somewhat fancier aluminum plug with an expanding cone retainer using an actual M3 nut, worked fine for the last year, but Mary recently noticed the socket head screw had worked loose.

    In the interim, I’d moved the Bafang thumb control from its original position on the crossbar to just above the rear shifter:

    Tour Easy - right handlebar control stack
    Tour Easy – right handlebar control stack

    Which moved the clamp on the shortened grip off the end of the handlebar tube, so I flipped the grip around, tightened the clamp, and installed the plug.

    Unfortunately, the grip ID is 4 mm larger than the tube ID, which meant the plug’s cone retainer was struggling to hold on in there. Perhaps the plastic cone has relaxed bit, but I figured giving it more traction would be a Good Idea™ before I declared victory:

    Handlebar Grip Sleeve - PrusaSlicer
    Handlebar Grip Sleeve – PrusaSlicer

    It’s a little plastic sleeve with slots to let it expand against the inside of the grip:

    Handlebar grip sleeve - installed
    Handlebar grip sleeve – installed

    Yes, it’s sticking out slightly; you can see the corresponding gap up inside next to the tube.

    A wrap of double-sided sticky tape glues it in place as the retainer presses it against the grip ID and a dot of low-strength Loctite should keep the screw from loosening again.

    The OpenSCAD source code:

    // Handlebar grip sleeve
    // Ed Nisley - KE4ZNU
    // 2025-10-25
    
    include <BOSL2/std.scad>
    
    /* [Hidden] */
    
    ID = 0;
    OD = 1;
    LENGTH = 2;
    
    HoleWindage = 0.2;
    Protrusion = 0.1;
    NumSides = 3*2*4;
    
    $fn=NumSides;
    
    Sleeve = [18.5,22.0,14.0];
    Kerf = 1.0;
    
      difference() {
        tube(Sleeve[LENGTH],id=Sleeve[ID],od=Sleeve[OD],anchor=BOTTOM);
        for (a=[0,90])
          zrot(a)
            up(Sleeve[LENGTH]/4)
              cuboid([2*Sleeve[OD],Kerf,Sleeve[LENGTH]],anchor=BOTTOM);
      }
    
    

    That was easy …

  • Monster Restocking

    Monster Restocking

    This being the season of monsters, I rebuilt and deployed a few from last year:

    Alligator - installed
    Alligator – installed

    Real spiders have better camouflage, but cardboard works pretty well:

    Spider 1 - camouflaged
    Spider 1 – camouflaged

    I must move them to the driveway on Friday:

    Spider 2 - camouflaged
    Spider 2 – camouflaged

    This one stands out in any situation:

    Green spider
    Green spider

    Tiny T-Rexes are just cute:

    Tiny T-Rex with pillar lamp
    Tiny T-Rex with pillar lamp

    They need support, because their heavy head bends the spine just above the hips, so they’re snuggled up against pillar lamps or each other:

    Mantis and Tiny T-Rexes
    Mantis and Tiny T-Rexes

    The cardboard Mantis turned out entirely too fragile:

    Mantis - dismantled
    Mantis – dismantled

    Reassembling the poor thing with a blob of hot-melt glue on each joint held it together.

    If I used something other than corrugated cardboard, they’d likely survive longer out there.

    A handful of RGBW tea lights provide just enough illumination to make them visible.

  • Mantis Durability

    Mantis Durability

    A Praying Mantis appeared on the house wall:

    Mantis - alert
    Mantis – alert

    The next morning found it huddled against the cold:

    Mantis - chilled
    Mantis – chilled

    It had reached operating temperature and gone about its business a few hours later.

    I deployed a cardboard Mantis in its honor as a seasonally appropriate yard decoration, but mine didn’t survive the night nearly as well as the real one:

    Mantis - dismantled
    Mantis – dismantled

    I doubt a predator was involved …

    A site search will reveal previous encounters with their kind.

  • Work Sharp Precision Adjust Sharpener: Button Improvement

    Work Sharp Precision Adjust Sharpener: Button Improvement

    A recent professional knife / lopper sharpening convinced me to up my sharpening game, so I figured a Work Sharp Elite sharpener would improve our backup blades:

    Work Sharp Knife Sharpener - overview
    Work Sharp Knife Sharpener – overview

    Protip: Wear gloves, because you’re working in front of an unprotected and eventually very sharp blade.

    The blade-holding clamp snaps magnetically into a rotating chuck so you can flip the knife over, at least if it’s not quite as long as that one. The chuck index has a spring-loaded release button:

    Work Sharp Knife Sharpener - rear view
    Work Sharp Knife Sharpener – rear view

    The spring is powerful and the button arrived with a recess around the screw holding the chuck together:

    Work Sharp Knife Sharpener clamp button - as received
    Work Sharp Knife Sharpener clamp button – as received

    Pressing the button hard enough to release the chuck hurt my index finger, but their Tech Support said it’s like that and that’s the way it is. Turning the screw adjusts the spring compression, but I think this situation calls for “more secure” rather than “easy to push”.

    Fortunately, I have a laser cutter and know how to use it:

    Work Sharp Knife Sharpener clamp button - filled
    Work Sharp Knife Sharpener clamp button – filled

    Despite appearances, it’s a 10 mm disk of 4.3 mm clear acrylic stuck to the screw head with a snippet of white double-sided tape and flush with the surrounding plastic surface.

    A smooth button makes my index finger much happier …

  • Fiskars Lopper Jaw Repair

    Fiskars Lopper Jaw Repair

    The Fiskars PowerGear lopper Mary uses in the garden had occasionally encountered a tomato cage wire and the blade had a few dents. We recently had a bunch of knives / blades / tools sharpened by somebody who knows what he’s doing and, while the lopper blade is now deadly sharp, grinding the dents out changed its shape enough that it no longer met the opposing plastic (probably glass-filled nylon) anvil.

    For lack of anything smarter, I cleaned the anvil, spread a layer of hot-melt glue over the surface, squished it flat with a snippet of PTFE fabric, and closed the jaws:

    Fiskars lopper jaw repair - silicone cloth indent
    Fiskars lopper jaw repair – silicone cloth indent

    Which left a blobular layer on both sides of the now perfectly matched blade channel:

    Fiskars lopper jaw repair - blade indent
    Fiskars lopper jaw repair – blade indent

    Trimming off the blobs made it slightly more presentable:

    Fiskars lopper jaw repair - trimmed edges
    Fiskars lopper jaw repair – trimmed edges

    The textured surface definitely looks great, even if the rest looks like the hack job it is.

    I’m hoping the glue layer has enough traction on the anvil to survive the duty it gets in the garden, where Mary uses it to harvest cabbages & suchlike. I’m sure the occasional cage wire will test its resolve, but we’ll know more next summer.