The Smell of Molten Projects in the Morning

Ed Nisley's Blog: Shop notes, electronics, firmware, machinery, 3D printing, laser cuttery, and curiosities. Contents: 100% human thinking, 0% AI slop.

Tag: Repairs

If it used to work, it can work again

  • Sonicare E5000 Toothbrush + Norelco T770 Beard Trimmer: Final Final Batteries

    Sonicare E5000 Toothbrush + Norelco T770 Beard Trimmer: Final Final Batteries

    Although replacing the Sonicare E5000 battery six years ago was supposed to be the last time I’d do that, the poor thing died leaving most of a year’s supply of brush heads in the drawer.

    Half a quartet of NiMH AA cells should keep it happy while using up that stash:

    Sonicare Toothbrush - NiMH AA cells installed
    Sonicare Toothbrush – NiMH AA cells installed

    The AA cells sit at a jaunty angle due to re-re-using the original contact tabs soldered into the PCB.

    I’m getting pretty good at taping the case closed:

    Sonicare Toothbrush - Kapton tape
    Sonicare Toothbrush – Kapton tape

    Although I have no pictures to prove it, the other half of the AA cell quartet restored youthful vigor to the Norelco T770 beard trimmer. Having interior pictures made finding and popping its case latches so much easier.

    If only I could change my batteries that easily …

  • Sears Humidifier: Bottle Patching

    Sears Humidifier: Bottle Patching

    Although the Sears humidifier (Model 758.154200 if you’re keeping score) that Came With The House™ works fine with its lid hinges broken, Mary heard an odd hissing sound somewhere inside. The sound continued with the thing unplugged and, after a protracted struggle in the kitchen sink, we tracked the sound to a crack in one of the dimples joining the front and back faces of the right-side water bottle:

    Sears Humidifier bottle - overview
    Sears Humidifier bottle – overview

    The vertical shaded bars come from the camera’s electronic shutter vs. unfiltered 60 Hz AC powering the shop LED lights.

    Unsurprisingly, replacement bottles are no longer available, although you can get fill caps and valves, plus wicking filters.

    A water drop squeezed in the crack:

    Sears Humidifier bottle - crack
    Sears Humidifier bottle – crack

    The bottles are polyethylene that sneers at any normal sealant, but I have a few square inches of tape intended for repairs exposed to weather. I didn’t get the snippet aligned just as I wanted, but its gooey adhesive definitely covered the crack:

    Sears Humidifier bottle - patched
    Sears Humidifier bottle – patched

    The bottles normally operate with a slight vacuum, thus the air hissing through the crack, so the tape need not withstand any continuous pressure and the adhesive layer should flow into the crack if it goes anywhere at all.

    Protip: the gooey adhesive bonds instantly and irrevocably to whatever it touches, so do a trial fit before you peel off the backing tape.

    If the “Serial” is a date code, it’s been around for while:

    Sears Humidifier - data plate
    Sears Humidifier – data plate

    It should be good for a few more decades …

  • Humidifier Lid Hinges

    Humidifier Lid Hinges

    The humidifier that Came With The House™ had a lid with two broken plastic hinges that I figured I could never replace, but while cleaning out the fuzz for the upcoming season I found one missing piece stuck inside the lid. Given a hint, I glued it back in place:

    Humidifier Hinge - outlined
    Humidifier Hinge – outlined

    There’s a strip of duct tape around the outside holding the fragment in place while the adhesive cured.

    A manual curve fit to the image in Inkscape produced the red outline, which gets saved as a plain SVG and fed into OpenSCAD to create a solid model:

    Humidifier Hinge - solid model
    Humidifier Hinge – solid model

    The cylinder doesn’t exactly fit the end of the hinge, but it’s close enough. The straightforward OpenSCAD code making that happen:

    // Humidfier Hinge Replacement
    // Ed Nisley KE4ZNU
    // 2024-10-20
    
    HingeThick = 10.0;
    PinLength = 10.0;
    
    ScrewOD = 2.0;
    
    NumSides = 2*3*4;
    Protrusion = 0.1;
    
    difference() {
        union() {
            translate([0,0,HingeThick])
                cylinder(d=6.0,h=PinLength,$fn=NumSides);
    
            linear_extrude(height=10.0,convexity=5)
                translate([-3.1,-8.0])
                    import("Humidifier Hinge - ouline.svg");
        }
    
        cylinder(d=ScrewOD,h=4*(HingeThick + PinLength),center=true,$fn=8);
    }
    

    The pin has a hole for a M2 screw, but contemplation of the broken pieces suggested the pin wasn’t the weakest link, which later experience confirmed.

    Figuring I’d need only one hinge, I made a spare for fitting:

    Humidifier hinge - on platform
    Humidifier hinge – on platform

    The unmodified part fit just about perfectly, whereupon a completely ad-hoc fixture involving a pair of laser-cut MDF slabs, a craft stick epoxy mixer, and more duct tape held it in place while the adhesive cured:

    Humidifier hinge - fixturing
    Humidifier hinge – fixturing

    The hinge pin turned out to be half a millimeter too long, which is easily fixed, and it worked fine:

    Humidifier hinge - installed
    Humidifier hinge – installed

    That’s more duct tape wrapped around the perimeter to hold the pieces in place, should it break again.

    Which, I regret to report, occurred on the way up the stairs from the Basement Shop™ when the lid slipped from my grasp, fell away from the rest of the humidifer’s top panel, and jammed open:

    Humidifier hinge - break
    Humidifier hinge – break

    The PETG-CF part held together, the adhesive remained bonded to both pieces, but the original plastic fractured just below the joint. A closer look from the other side shows the break:

    Humidifier hinge - break detail
    Humidifier hinge – break detail

    The other hinge broke about where it did before.

    So the humidifier remains in service with the lid in status quo ante and a small bag inside holding the fragments for the next return to the shop.

    Drat!

  • Worst Deck Staining Job Ever

    Worst Deck Staining Job Ever

    This looks about as awful as I expected:

    Worst deck staining job ever
    Worst deck staining job ever

    The previous owners replaced the deck two years ago, but the contractor installed more than half the planks with the grain cupped upward. The job was so bad the contractor replaced the most egregiously warped planks (over by the door and out of sight on the right) under warranty, but left all the other mis-oriented planks in place, presumably because they weren’t that bad yet.

    The bare wood must age for a while before staining, so the shelf of painting supplies held a year-old gallon can as a reminder, with about two inches of stain / preservative in the bottom. I applied it to the “new” planks with pleasing results that absolutely do not match the rest of the weathered wood. With nothing to lose and plenty to gain, I applied the rest of the potion to the worst of the upside-down planks, producing the egregiously bad result you see above.

    Given how the stain weathered to oblivion over the course of the last year, I expect all those planks will become roughly the same shade of ugly by next summer, when I might possibly be motivated to slather another gallon over the deck.

    A friend observes: Houses are trouble.

  • EBL Bucked Lithium AA and AAA Cells

    EBL Bucked Lithium AA and AAA Cells

    A new kitchen scale eats a quartet of AAA alkaline cells every month, so a set of bucked lithium AAA cells make sense:

    EBL AAA first charge - 2024-09-11
    EBL AAA first charge – 2024-09-11

    The cells claim 1200 mA·hr capacity, because it looks much more impressive than 1.2 A·hr, and deliver 900 mA·hr at 500 mA, likely higher than the scale’s actual load current.

    The old Sony DSC-H5 works well with the light box and gets a pair of bucked lithium AA cells to replace the tired Eneloops:

    EBL AA first charge - 2024-10-17
    EBL AA first charge – 2024-10-17

    They claim 3000 mA·hr and deliver 2.5 A·hr at 500 mA: nearly perfect, considering some of the junk I’ve gotten over the years.

    Now, to see how they behave in real life …

  • Gizo Spiders: Leg Splice

    Gizo Spiders: Leg Splice

    This being the season for decorative spiders, two more appeared:

    Gizo spider assortment
    Gizo spider assortment

    Wedding photographers have trouble getting the proper exposure for both the bride and the groom, too.

    Only one of the 32 legs came loose from the platform:

    Gizo spider - failed leg
    Gizo spider – failed leg

    The upper part of the leg captured the loose segment and glommed it into a blob:

    Gizo spider - failed leg - detail
    Gizo spider – failed leg – detail

    Fortunately, one of the clearance test pieces was an isolated leg and joint, so I amputated the grisly mess, matched the cut in the test piece, and hot-melt-glued the pieces together:

    Gizo spider - spliced leg
    Gizo spider – spliced leg

    Not quite perfect, but good enough for the purpose.

    Given the 3% failure rate, I think the legs show such small contact areas really do justify a brim. Adding a brim to the main body would mess up the joints, but I think PrusaSlicer can add brims to specific parts. More study is needed.

    Orange eyes for the win!

  • Seasonally Appropriate Teapot Knob

    Seasonally Appropriate Teapot Knob

    Long years ago, the Bakelite (or some such) lid on our rarely used teapot disintegrated, whereupon I replaced it with an aluminum sheet and metal knob. Admittedly, a metal knob was not the brightest idea I ever had, but it sufficed for a few uses over the intervening decades.

    Mary hosted this month’s quilting bee and, after having someone else bring a larger teapot for the occasion, suggested I Make. A. Better. Knob. After a bit of searching, this statue seemed appropriate for the season:

    Skull teapot knob
    Skull teapot knob

    It’s printed with PETG filament that should easily withstand the no-more-than-boiling-water temperatures found atop a teapot.

    I imported the original model into PrusaSlicer, shrank it to 50 mm tall and simplified the mesh, exported it as an OBJ file, imported it into OpenSCAD, mashed it together with a 1/4-20 threaded_nut from BOSL2, added the finger protector, and got a suitable model:

    Teapot Knob - solid model bottom view
    Teapot Knob – solid model bottom view

    The as-printed threads were a bit snug with $slop=0, but running the screw in with a dot of silicone grease to ease the way worked fine.

    I should rebuild the whole lid in PETG-CF sometime.

    The OpenSCAD code stitches the parts together:

    // Teapot Knob
    // Ed Nisley - KE4ZNU
    // 2024-10-11
    
    include <BOSL2/std.scad>
    include <BOSL2/threading.scad>
    
    StackHeight = 50.0;
    ThreadLength = 25.0;
    HeatbreakOD = 40.0;
    HeatbreakThick = 3.0;
    
        intersection() {
            union() {
                cylinder(d=HeatbreakOD,h=HeatbreakThick,$fn=2*4*9);
                up(HeatbreakThick)
                    translate([-121,-105])      // totally eyeballometric
                        import("stackofskulls - 50mm.obj",convexity=10);
            }
    
            union() {
                threaded_nut(100,INCH/4,ThreadLength,INCH/20,        // flat size, root dia, height, pitch
                                         bevel=false,ibevel=false,anchor=BOTTOM);
                up(ThreadLength)
                    cylinder(d=100,h=StackHeight);
            }
        }