Ed Nisley's Blog: Shop notes, electronics, firmware, machinery, 3D printing, laser cuttery, and curiosities. Contents: 100% human thinking, 0% AI slop.
I finally made a test bar to line up the (vertically mounted) rotary table and tailstock on the Sherline milling machine. It’s a ground-and-polished 0.500-inch rod from a defunct HP2000C inkjet printer; the print head zipped back and forth along the rod while printing, so you know it’s pretty smooth. You could probably salvage something similar from any dead inkjet printer.
Making the bar is simple: saw off a suitable length, stick it in the lathe, face off the end, chamfer the edge, poke a center drill into it, and it’s all good.
If you’re a tool-and-die jig-boring high-precision kind of machinist, you better stop reading right about now before you catch a heart attack.
Lining the bar up is almost trivially easy with a laser spot coming down the spindle bore. Move the table so the spot grazes the side of the bar and casts a shadow on the table, jog X to the other end of the bar, and tweak the angle for the same picture on the table.
Repeat until satisfied.
The trouble comes at the tailstock end, where the ram extends about 1.5 inches, tops. That’s good enough for the Sherline, but it also means the test bar must be pretty close to the length of whatever you’ll be machining, rather than as long as possible to get the best alignment.
However, after you get Sherline tailstock aligned to the end of the bar, vertically, horizontally, and angularly, the magic happens
The ram is quite stable, with very little radial play, so the point moves along the X axis (assuming you did a good job aligning the tailstock). Retract the ram a bit, jog X and Y to put the laser spot on the tip of the center (which should correspond to the Y axis coordinate of the center of the bar), and you’ll see a defocused spot on the table (I put a white card on the table to improve the contrast). Jog Z until there’s a nice triangular image of the dead center’s point in that bright round spot.
It turns out that the laser beam in the top picture is about 10 mils wide at the dead center axis, so you can easily see a difference of 1 mil in the Y coordinate. That’s perfectly accurate for the sort of work I do.
Now, remove the test bar, unclamp the tailstock, move it to wherever you need it for the actual thing-to-be-made, snug it down, and jog the table in X (only!) to move the spot over there, too. Move the tailstock around to align the image of the center point in the middle of the laser spot again and you can be sure it’s aligned to the same Y coordinate. Verify that the tailstock has the same angular alignment. Mine is consistent with the T-nuts pressed against the front of the table slots and it’s easy to slide it carefully along the Y axis to get the point in the spot.
Because the bar was parallel to the X axis to start with, the point is now aligned with the axis of the rotary table.
Laser spot focused on tip
The minimum spot size depends on the beam width and the lens, but it turns out that for my setup, twiddling the Z position of the lens can shrink the spot down to essentially the width of the dead center point. As nearly as I can tell, the beam width is 3 mils and the point pretty much occludes the beam when it’s properly aligned.
The picture shows that situation; the spot is half-occluded because the point now looks like the side of a barn. It’s difficult to tell, but the lens (on the brass snout in the endmill holder) is lower in this picture.
All that jogging, particularly creeping up on the proper alignment, goes much easier with a joggy thing!
After replacing the seat strut screws, I found a Round Tuit lying there on the workbench, right next to the rear reflectors I’ve been meaning to install for a truly embarrassing period.
Recumbents don’t have the usual assortment of standard-sized tubing in the usual road-bike places, making common items like reflectors difficult to attach. The ideal spot on our bikes is at the base of the VHF/UHF antennas, right next to the white blinky LEDs, but, alas, that’s 20 mm in diameter and the reflector clamp barely shrinks down to a bit under 28.
Turns out that a chunk of 1.5 inch PVC pipe has a 4 mm wall thickness, so wrapping a layer of that around the antenna base will do the trick. I whacked off a length of pipe, faced off both ends in the lathe, and put a shallow recess around the middle of the ring to capture the reflector clamp.
By another rare coincidence, 1.5 inch PVC pipe has an ID of exactly 40 mm… so cutting the ring exactly along a diameter produces the right length. The catch is that the pipe isn’t flexible at all, but brandishing a heat gun in a threatening manner solves that problem.
Reshaped bushing on mandrel
A random hunk of 3/4-inch aluminum rod is about 19 mm in diameter, so I chucked that in the lathe and shaped the saggy strip around it… wearing thick leather gloves.
It springs out to 20 mm with no problem, slides right on, and grips reasonably well. I may add a strip of tapeless sticky (think double-sided tape without the tape: just the adhesive!) under the bushing if it wants to walk away.
I made two of ’em, of course, and put a reflector on Mary’s bike while I was at it. Our young lady’s bike already has a reflector, although I should upgrade that bushing as well… it’s a layer of self-vulcanizing rubber tape that works perfectly, so this may take a while.
I suppose I should buy a length of gray or black PVC pipe, but that’s in the nature of fine tuning.
Straight up: this is about a stainless steel socket head cap screw I installed eight years ago, not the original Easy Racers screw, so this is not their problem.
I rode out for milk-and-eggs at the corner store, a flat one-mile ride, and stopped at the traffic signal. Light goes green, line of cars accelerates, so do I… and there’s a snap and the left side of the seat sags backwards. I am not a powerhouse rider and it’s March, so I’m not doing leg presses while getting up to cruising speed.
I continued the mission by sitting slightly to the right on the seat and pedaling gingerly, then diagnosed the problem in the corner store’s parking lot. If I’d been further away, I’d have done the repair right there, but I figured it’d hold together until I got home. It did.
The problem turned out to be a broken screw holding the left-side seat strut to the threaded eyelet on the rear dropout. The top picture shows the way I have it set up: seat strut clamp outboard, rack strut inboard, with a socket head cap screw extending all the way through, and secured with a pair of stainless nuts that went missing along with the broken screw end.
Screw fracture closeup
Here’s the fracture across the end of the screw, which shows no evidence of foul play. As nearly as I can tell, the whole thing snapped off in one event, with none of the crud that would indicate a progressive crack. Compared with that wheel stud, this is in pristine condition.
So it’s time to replace the right-side screw, as well, which means a trip to the Bike Repair Wing of the Basement Laboratory. While I had the bike up in the repair stand, I decided to reshape the head on the right-side screw for better chain clearance.
As nearly as I can tell, the usual practice puts both the seat strut and the rack strut outboard of the threaded eyelet on the dropout, but that seems wrong to me. The seat strut puts a tremendous amount of stress on the screw, so you really want that lever arm as short as possible: put the clamp against the eyelet. While the rack isn’t as heavily loaded, cantilevering it outboard of the clamp just doesn’t look right.
But putting the rack strut inboard of the eyelet means the screw head sticks out rather more than I’d like. Very rarely, the chain will snick against the head and even more rarely it jams between the head and the freewheel. Nothing much happens (it’s a freewheel, after all), but I think reducing the head thickness ought to help.
Reshaped socket head cap screw
So I chucked the screw in the lathe, shortened the socket by about half, and put a taper on the head. If I had a stock of round-head cap screws, one of those would be even better.
The shortened socket makes it a bit tricky to get enough bite with the hex key, but this isn’t something that requires much attention after it’s installed… and I get to do all that in the shop.
Dabs of Loctite in the eyelet and nuts, for sure!
By a truly rare coincidence, a standard 1-1/2 inch cap screw is exactly the right length.
Right-side mount
Here’s a view of the installed right-side screw, looking rearward along the upper rear triangle tube. Seat strut to the outside, rack strut to the inside, and reshaped head above the cluster.
Took the bike out for a 16 mile spin today and it’s all good.
A note for the weight weenies in the crowd: a rack on the back of the seat adds a redundant support structure. Without that, a failed seat strut can be a real showstopper. Even if you don’t use your bike as a pack mule, maybe you should add a rack.
Nothing like sleeping on a problem. It turns out that a chunk of HAL code can do a nice job of locking out an inactive joystick axis.
The general idea:
A priority encoder selects one axis when both go active simultaneously
The prioritized outputs set flipflops that remember the active axis
The active axis locks out the other one until they’re both inactive
That way, you can start to jog either axis on a knob without worrying about accidentally jogging the other axis by moving the knob at a slight diagonal. I hate it when that happens.
The other tweak is that the quartet of buttons on the right act as a “hat” for the Z and A axes, jogging them at the current maximum speed.
Because it’s tough to accidentally push two buttons at once, there’s no need to lock them out. So you can jog diagonally by deliberately pushing adjoining buttons, but you must want to do that.
Rather than dumping the whole program again, here are the key parts…
Figuring out if a joystick axis is active uses the window comparators. It seems the idle counts value varies slightly around 127, so I relaxed the window limits. Should the window comparator go active with the knob centered, the buttons for that axis won’t produce any motion.
net x-jog-count-int input.0.abs-x-counts conv-s32-float.0.in
net x-jog-count-raw conv-s32-float.0.out wcomp.0.in
setp wcomp.0.min 125
setp wcomp.0.max 130
net X-inactive wcomp.0.out not.0.in
net X-active not.0.out
The priority encoder is just a gate that prevents Y (or A) from being selected if X (or Z) is simultaneously active. Here’s a sketch for the ZA knob:
Axis priority encoder
The active and inactive signals come from the window detectors. The sketch gives the K-map layout, although there’s not a whole lot of optimization required.
The corresponding code:
net Z-inactive and2.5.in0
net A-active and2.5.in1
net A-select and2.5.out # select A only when Z inactive
net Z-inactive and2.6.in0
net A-inactive and2.6.in1
net ZA-Deselect and2.6.out # reset flipflops when both inactive
net Z-active and2.7.in0 # set Z gate when knob is active
net A-gate-not and2.7.in1 # and A is not already gated
net Z-set and2.7.out flipflop.2.set
net ZA-Deselect flipflop.2.reset # reset when neither is active
net Z-gate flipflop.2.out not.6.in
net Z-gate-not not.6.out
net A-select and2.8.in0 # set A gate when knob is active
net Z-gate-not and2.8.in1 # and Z is not already gated
net A-set and2.8.out flipflop.3.set
net ZA-Deselect flipflop.3.reset # reset flipflop when both inactive
net A-gate flipflop.3.out not.7.in
net A-gate-not not.7.out
The flipflops remember which axis went active first and lock out the other one. When both axes on a knob return to center, the flipflops reset.
The quartet of buttons produce binary outputs, rather than the floats from the Hat, so a pair of multiplexers emit -1.0, 0.0, or +1.0, depending on the state of the buttons, for each axis.
setp mux2.6.in0 0.0
setp mux2.6.in1 -1.0
net A-btn-neg input.0.btn-trigger mux2.6.sel
net A-btn-neg-value mux2.6.out sum2.1.in0
setp mux2.7.in0 0.0
setp mux2.7.in1 1.0
net A-btn-pos input.0.btn-thumb2 mux2.7.sel
net A-btn-pos-value mux2.7.out sum2.1.in1
net A-jog-button sum2.1.out
net A-btn-neg or2.1.in0
net A-btn-pos or2.1.in1
net A-btn-any or2.1.out or2.2.in0
net A-gate or2.2.in1
net A-motion or2.2.out
The A-motion signal is true when either of the A jog buttons or the A joystick axis is active. That gates the MAX_ANGULAR_VELOCITY value to halui.jog-speed, rather than the default MAX_LINEAR_VELOCITY. Or, depending on the state of the toggle from the two joystick push switches, 5% of that maximum. A mere 5% may be too slow for the A axis, but it’ll take some experience to determine that.
With that in hand, the final step is gating either the knob or the button values to halui.jog.*.analog.
net Z-jog-button mux2.8.in0
net Z-jog-knob-inv mux2.8.in1
net Z-gate mux2.8.sel
net Z-jog mux2.8.out halui.jog.2.analog
net A-jog-button mux2.9.in0
net A-jog-knob input.0.abs-z-position mux2.9.in1
net A-gate mux2.9.sel
net A-jog mux2.9.out halui.jog.3.analog
The Hat jogs X and Y at the current maximum speed.
The Left Knob jogs X and Y proportionally to the Knob displacement.
The Right Knob jogs Z (Up-Down) and A (Left-Right) proportionally to the Knob displacement.
Press either Knob downward to toggle the maximum jog speed between MAX_LINEAR_VELOCITY (as defined in the Sherline.ini file) and 5% of that value. The slow speed is useful for creeping up on alignment points: the first active level of the joysticks runs at a nose-pickin’ pace.
The left little button (labeled 9) switches to Manual mode, although the AXIS display does not update to indicate this. Same as “F3” on keyboard, minus the GUI update.
The right little button (labeled 10) continues a G-Code program by activating the Resume function. Same as “S” on the keyboard.
The Mode button switches the functions of the Hat and Left Knob. That button does not generate an output and the Mode cannot be controlled programmatically. Swapping those functions doesn’t seem particularly useful in this application, so the LED should never be ON.
Buttons 1-4 are not used for anything yet.
On the back:
Pressing the left-hand pair of buttons (labeled 5 and 7) activates E-stop. Yes, I know all about why you shouldn’t have E-stop run through software. This is a Sherline mill. Work with me here.
The right-hand buttons (labeled 6 and 8) do nothing yet.
The code…
In Sherline.ini:
[HAL]
HALUI=halui
In custom.hal:
loadusr -W hal_input -KA Dual
All the heavy lifting happens in custom_postgui.hal. As nearly as I can tell, HAL is basically a write-only language, so there’s block diagram of the major chunks of “circuitry” down at the bottom.
First, some setup and the simple buttons:
#--------------
# Logitech Dual Action joypad
loadrt and2 count=3
loadrt conv_s32_float count=3
loadrt mux2 count=2
loadrt or2 count=1
loadrt scale count=4
loadrt sum2 count=2
loadrt toggle count=1
loadrt wcomp count=3
#-- central buttons activate manual mode and restart the program
net mode-manual input.0.btn-base3 halui.mode.manual
net pgm-resume input.0.btn-base4 halui.program.resume
#-- left-hand rear buttons active estop
addf and2.0 servo-thread
net pgm-estop-0 input.0.btn-base and2.0.in0
net pgm-estop-1 input.0.btn-top2 and2.0.in1
net pgm-estop and2.0.out halui.estop.activate
Because the Left Knob and Hat will never be active at the same time, a sum2 block combines the two controls into single value (separate for X and Y, of course). Each sum2 input has a separate gain setting, which is a convenient place to adjust the Y axis sign.
#-- left knob runs XY at variable rate
# hat runs XY at full throttle
addf sum2.0 servo-thread
net x-jog-knob input.0.abs-x-position sum2.0.in0
setp sum2.0.gain0 +1.0
net x-jog-hat input.0.abs-hat0x-position sum2.0.in1
setp sum2.0.gain1 +1.0
net x-jog-total sum2.0.out halui.jog.0.analog
addf sum2.1 servo-thread
net y-jog-knob input.0.abs-y-position sum2.1.in0
setp sum2.1.gain0 -1.0
net y-jog-hat input.0.abs-hat0y-position sum2.1.in1
setp sum2.1.gain1 -1.0
net y-jog-total sum2.1.out halui.jog.1.analog
The Right Knob values go through scale blocks to adjust the polarity. Note that the Gamepad’s rz axis controls the EMC2 Z axis and Gamepad z controls the EMC2 A axis. Basically, it made more sense to have up-down control Z and left-right control A.
#-- right knob runs Z at variable rate (front-back)
# A (left-right)
addf scale.0 servo-thread
net z-jog-knob input.0.abs-rz-position scale.0.in
setp scale.0.gain -1
net z-jog-total scale.0.out halui.jog.2.analog
addf scale.1 servo-thread
net a-jog-knob input.0.abs-z-position scale.1.in
setp scale.1.gain +1
net a-jog-total scale.1.out halui.jog.3.analog
There’s only a single halui.jog-speed setting, but the jog speeds for the linear axes and the angular axes differ by so much that Something Had To Be Done. As above, I assumed that only one of the axes would be jogging at any one time, so I could set halui.jog-speed to match the active axis.
A window comparator on each linear axis detects when the joystick is off-center; the output is 1 when the axis is centered and 0 when it’s pushed. Combining those three signals with and2 gates gives a combined linear-inactive signal.
A mux2 block selects the MAX_ANGULAR_VELOCITY from the ini file when linear-inactive = 1 (linear not active) and MAX_LINEAR_VELOCITY when it is 0 (any linear axis off-center).
Done that way, rather than detecting when the angular axis is off-center, means that inadvertently activating the angular axis during a linear jog doesn’t suddenly boost the linear speed. Given that the max linear is about 28 inch/minute and the max angular is 2700 degree/min, it’s a pretty abrupt change.
I’m thinking about adding + shaped gates to at least the Right Knob so I can’t inadvertently activate both Z and A. I’m sure there’s a HAL lashup to do the same thing, though.
#-- set jog speed by toggle from either knob button
# press any knob button to toggle
addf and2.1 servo-thread
addf and2.2 servo-thread
addf conv-s32-float.0 servo-thread
addf conv-s32-float.1 servo-thread
addf conv-s32-float.2 servo-thread
addf mux2.0 servo-thread
addf mux2.1 servo-thread
addf or2.0 servo-thread
addf scale.2 servo-thread
addf scale.3 servo-thread
addf toggle.0 servo-thread
addf wcomp.0 servo-thread
addf wcomp.1 servo-thread
addf wcomp.2 servo-thread
#-- determine if any linear knob axis is active
net x-jog-count-int input.0.abs-x-counts conv-s32-float.0.in
net x-jog-count-raw conv-s32-float.0.out wcomp.0.in
setp wcomp.0.min 126
setp wcomp.0.max 128
net x-jog-inactive wcomp.0.out and2.1.in0
net y-jog-count-int input.0.abs-y-counts conv-s32-float.1.in
net y-jog-count-raw conv-s32-float.1.out wcomp.1.in
setp wcomp.1.min 126
setp wcomp.1.max 128
net y-jog-inactive wcomp.1.out and2.1.in1
net xy-active and2.1.out and2.2.in0
net rz-jog-count-int input.0.abs-rz-counts conv-s32-float.2.in
net rz-jog-count-raw conv-s32-float.2.out wcomp.2.in
setp wcomp.2.min 126
setp wcomp.2.max 128
net z-jog-inactive wcomp.2.out and2.2.in1
#-- convert ini file unit/sec to unit/min and scale for slow jog
setp mux2.0.in0 [TRAJ]MAX_LINEAR_VELOCITY
setp mux2.0.in1 [TRAJ]MAX_ANGULAR_VELOCITY
net linear-inactive and2.2.out mux2.0.sel
The ini file velocities are in units/second, so a scale block multiplies by 60 to get units/minute.
Another scale block multiplies by 0.05 to get slow-speed jogging. Obviously, that value is a matter of taste: tune for best picture.
Those two values go into a mux2 driven by the output of a toggle triggered by the or2 of the two buttons under the Knobs. Pushing either Knob down flips the toggle.
setp scale.2.gain 60
net jog-per-sec mux2.0.out scale.2.in
net jog-per-min scale.2.out mux2.1.in0
net jog-per-min scale.3.in
setp scale.3.gain 0.05
net jog-per-min-slow scale.3.out mux2.1.in1
net xy-button input.0.btn-base5 or2.0.in0
net za-button input.0.btn-base6 or2.0.in1
net xyza-button or2.0.out toggle.0.in
net xyza-slowmode toggle.0.out mux2.1.sel
net axis-jog-speed mux2.1.out halui.jog-speed
When the jog speed is at the maximum allowed, it still gets trimmed by the per-axis limits, so you can’t over-rev the motors no matter how hard you try. Even better, changing the values in the ini file automagically affect the gamepad jog speeds.
Here are the pin names for a Logitech Dual Action USB (wired) gamepad, according to EMC2 2.3.4. You’ll need these to wire it up as a control pendant for your EMC2 CNC milling machine…
There’s no need for -KRAL because it has no programmable LEDs.
Prefix all these with input.0. to get the complete name.
Hat Left-Right
abs-hat0x-counts
abs-hat0x-position
Hat Up-Down
abs-hat0y-counts
abs-hat0y-position
Hat Push
none
Left Knob Left-Right
abs-x-counts
abs-x-position
Left Knob Up-Down
abs-y-counts
abs-y-position
Left Knob Push
btn-base5
Right Knob Left-Right
abs-z-counts
abs-z-position
Right Knob Up-Down
abs-rz-counts
abs-rz-position
Right Knob Push
btn-base6
Button 1
btn-trigger
Button 2
btn-thumb
Button 3
btn-thumb2
Button 4
btn-top
Button 5
btn-top2
Button 6
btn-pinkie
Button 7
btn-base
Button 8
btn-base2
Button 9
btn-base3
Button 10
btn-base4
Mode button
swap Hat & Left Knob
lights red LED
All of the buttons have -not output pins.
The Knob position values run from -1.0 to +1.0 (float) and rest (almost) at 0.0 when centered. Their counts (s32) run from 0 to 255 and rest at 127 when centered.
The Hat button position values are only -1.0 and +1.0, centered at 0.0. The counts are only -1 and +1, with 0 when un-pushed. Although they take on only integer values, the position values are floats.
Both Knobs and the Hat have -Y position values at the top and +Y values at the bottom, exactly backwards from what you want. Expect to reverse the Y axis sign when you write the HAL code.
The -X position values are to the left, where you want them.
Although there’s a tactile click when pushing the Hat straight down, there is no corresponding button output. I don’t know if this is an oversight in the HAL interface or if there’s no actual switch in there.
The Mode button swaps the Hat and Left Knob functions. With the red LED on, both the Hat and Knob axes produce only -1 and +1 position and counts values.
A guide to figuring this stuff out is there, with useful pointers elsewhere on the main doc page.
The case for the Totally Featureless Clock is exactly what you’d expect: a solid black acrylic block with a Lexan Graylite faceplate. All you see are digits… no buttons, no knobs. Just the time, all the time.
I’d hoped to just epoxy the faceplate on and be done with it, but the edges really didn’t look right. A bit of rummaging turned up a Dremel 125 “High Speed Cutter” that looked to be exactly the right hammer for the job.
Dremel conical cutter in drill chuck
The Sherline CNC mill just doesn’t have the reach for a foot-long cut, so I clamped the case to the manual mill and grabbed the cutter in an ordinary drill chuck. This is absurd, but ya gotta run with what ya got…
According to the Dremel specs, the cutter should run at 20-30 k RPM, but, trust me on this, the mill doesn’t go that fast. I set it for 2000 RPM, the fastest it’s run in years, and hoped for the best.
The runout was breathtaking.
I aligned the case against against a parallel in one of the T-slots, which got it surprisingly close. A trial cut showed it was off by a bit, but two slight realignments (loosen clamps, slide gently, reclamp) and trial cuts put it spot on. That worked fine for three sides.
The cutter is about 6.3 mm dia and just over 9 mm long, so the cutting edge is inclined at almost exactly 1:3. That means a horizontal misalignment of 10 mils causes a vertical misalignment of 30 mils. Conversely, you can measure the vertical error and then tweak the horizontal to make the answer come out right.
Tweaking the alignment
The fourth side was off enough to make the final joint to the first side pretty ugly. I measured the vertical offset at about 80 mils, set the front magnetic block as a pivot and stuck a 25-mil feeler gauge between the rear block and the case. Remove the feeler, loosen the clamps, rotate the case, reclamp, and the cut was just about perfect. Certainly within my tolerances for such a thing… you can’t see it unless you’re looking for it.
The bottom picture shows the final bevel, hot off the mill table, minus the protective plastic wrap and plus a bunch of dust and adhesive smudges from the wrap. The end plate gives the vertical line down the right side and a slight discontinuity where it’s a few mils shy of the side. There’s a hairline around the whole case where the faceplate joins the black acrylic; I used transparent epoxy and a light weight to clamp the faceplate down, so the joint is uniformly thin all around.
A few passes on a sanding block ought to get rid of the tool marks and spiff the bevel up just fine all around.