Ed Nisley's Blog: Shop notes, electronics, firmware, machinery, 3D printing, laser cuttery, and curiosities. Contents: 100% human thinking, 0% AI slop.
Mary’s feet are exquisitely sensitive to irregularities in the insoles of her shoes, which poses a real problem with her bike shoes: those SPD cleat recesses are no good at all.
This is a view down into one shoe, with the SPD cleats adjusted all the way to the rear. That leaves a large recess in the front, which was painfully obvious to her sole. The white shape is the gap filler…
I pressed a sheet of paper across the gap to get the general shape, traced it twice onto a slab of 0.060-inch aluminum with a nice pebbly paint job, and cut the two pieces out. A few conversations with Mr Belt Sander, a few licks with a rat-tail file, and they dropped right onto place. The recess is slightly curved, but I didn’t have to bend the pieces to fit.
I laid duct tape across the whole affair, put the insoles back in place, and it was all good.
The backing plate is 0.072 inch thick and she was content with the difference.
In previous shoes, with the cleat near the middle of the adjustment range, I’ve stuffed epoxy putty into the gaps. That works, but it doesn’t bond to the (miracle engineering plastic) soles and tends to crumble. This is Not A Good Thing…
The discussion following that post prompted me to take a closer look at the corroded spider. I planned to pull the spider off the back of the drum and examine the pieces, but a week of dribbling thread lube around the bolts left two of them firmly affixed.
While I don’t have it completely apart yet, some observations are in order…
Spider mounting bolts through drum
The bolts are stainless steel and utterly immovable with the usual screwdriver-handle-mounted Torx bit. I got the first two bolts out by putting a T30 bit in a 1/4-inch socket in a ratchet wrench and applying brute force.
A few days of thread lube (the incomparable PB B’Laster) persuaded two more out of their lairs. The remaining bolts may require even more brute force, but I’ll give the lube a few more days to work its magic.
Despite that, the bolts and holes are not corroded. They may have some thread locker down in there, but I see little evidence of that. I think it’s just a case of being torqued down hard, then set adrift in ionic water for half a decade.
The outer third of each arm has a covering of corrosion products, but the metal below that (now dried and flaking) gunk seems undamaged. The arms have severe corrosion and cracking throughout the inner two-thirds of their length.
Spider corrosion
If this were chemical corrosion, I’d expect it to apply evenly throughout the length of the arm, because the presence of corrosion products over the entire arm indicates pretty good distribution.
However, galvanic corrosion should follow the same pattern, so I’m not sure what to make of this.
The fact that an oxidation layer on the stainless steel tends to passivate it may not really matter. Compare the surface areas of the drum and the spider: there’s a whole lot more drum than spider, so even a passivated drum could provide enough current to rot the spider.
The ends of the spider spend their lives whipping through the water inside the tub at a pretty good clip. That could dislodge most of the crud and leave them reasonably clean, at least compared to the hub that moves more slowly (same rotational speed, smaller radius). It’s also true that the water level never reaches the hub, remaining below the level of the door seal.
Thus, the hub probably gets splashed, but never immersed, and thus has no way to remove any contaminants. The corrosion products simply build up there, keeping it wet throughout its life.
I maintain there’s little drying going on, even with the door open, in the relatively short intervals between washings. The hub region would be least likely to dry, however, because there’s absolutely no ventilation back there.
All that notwithstanding, this corrosion should not happen.
I’d very much like to see some measurements: we’re all obviously guessing at the conditions. The plastic tub surrounding the drum has a port for the rear vent near the perimeter, so it’s possible to get a (cramped, inconvenient) look in there without tearing the washer apart.
Somehow I managed to shred the silicone cushion of the earbud on my bike radio. As nearly as I can tell, it got caught between the seat and the back; the missing part certainly isn’t inside my ear.
Anyhow, I have a bag of spare cushions from all the other earbuds, so this isn’t a showstopper.
The adhesive snot holding the earwax filter in place also failed, so I figured I should fix that while I had the hood up. The old filter was all ooky with earwax & oil & dried sweat, which meant that any new adhesive wouldn’t stick. I chopped a disk from a random foam earbud cover with a 7/32-inch hollow punch and glued it in place with some acrylic sealant.
Earbud cushion and wax filter replacement
While I had the sealant out, I replaced the tape sealing the vent hole (on the other end of the earbud) with a dot of glop, much as I should have done originally.
I’ve managed to lose enough weight off my butt (it doesn’t go away, it just becomes leg muscle for a few months) that I must move the seat on my Tour Easy forward maybe 5 mm. Alas, I’ve run out of adjustment room: the frame is a Medium Large and I probably should have gotten a Medium; that decision was forced by getting a much-too-small Linear many years ago.
The general idea here is to bolt the seat to an aluminum circumferential clamp just forward of the plate and tubes that normally secure the seat to the frame. That moves the clamping bolts about 15 cm forward, but they slide in slots along the seat bottom.
The bolts are 1/4-20 stainless carriage bolts, with the square shank under the head sliding in those slots. I think the clamp can be about the same thickness as the existing tubes, so the same bolts will work.
The main frame tube runs slightly above the two small tubes that stiffen the rear triangle. It’s not clear those clearances in the clamp must be contoured to fit the tubes exactly; a simple flat cutout will probably work just fine.
The top of the clamp must have two bosses to support the seat base around the clamping screws. A line of rivets down the middle secures the seat base to the contoured (carbon?) fiberglass pan holding the foam cushion.
With the jack in hand, I idly poked a coaxial plug into it and realized that the amount the plug stuck out was just about exactly equal to the thickness of the black plastic cap on its tip. Some rummaging turned up one of the six plugs with a missing tip, at which point both the problem and its solution were obvious.
Broken vs original coaxial power tips
A bit of tedious work with a tiny screwdriver and a needle convinced the socket to disgorge the plastic ring from its bowels …
Broken tip extracted from jack
Now, I suppose I could have figured this out without taking the case apart, but actually fixing the problem would still require surgery, soooo there’s no wasted effort. That’s my story and I’m sticking with it.
If you think you could extract that ring from the outside, there’s a joke about that.
I put the case back together with a few dabs of silicone snot adhesive (despite what I know about letting acetic acid loose near electronics) to anchor the circuit board, applied a belly band of tastefully color-coordinated (i.e. silver) duct tape, and it’s all good.
Actually, the pack was stone cold dead until I plugged it into the charger to reset its battery protection circuitry. Evidently, disconnecting and reconnecting the battery tripped the protection logic. I’ve seen that in other Li-Ion packs, so it wasn’t quite so scary as it was the first time around.
As for the coaxial power tip: a dab of solvent glue, an overnight clamping session, and I think it’ll work fine forever more.
I should machine up some stabilizing collars around the sockets to match that obvious shoulder on the plug, shouldn’t I?
The power lead into the Li-Ion pack I’m using for the bike radio became badly intermittent on a recent ride. When I got back I swapped in a different pack and the problem Went Away, but I noticed that the coaxial power plug didn’t seem to seat all the way into the jack on the failed pack. I’d noticed that before, although I attributed it to getting two different sets of the packs; it didn’t seem to make any difference.
Given that I was going to have to either repair or replace the jack, dismantling the offending pack was next on the list. Some preliminary poking showed that there were no screws concealed under the label, so the two halves of the pack were either snapped or bonded together.
The case didn’t respond to the usual wedging and prying by revealing an opening, which suggested that it was bonded. That meant I must saw the thing apart.
I set up a 31-mil slitting saw on the Sherline and clamped the pack atop a random plastic slab atop the tooling plate. The Sherline’s limited throat depth meant I had to cut the far side of the pack. I aligned the saw to the Z-axis level of the joint along the middle of the pack by eyeballometric guesstimation.
Slitting saw setup
Key point:
You absolutely do not want to saw into a lithium-ion cell, not even a little bit.
Therefore:
The pack must be aligned parallel to the cutter’s travel
The cuts must proceed in tiny increments, and
You must verify that each cut doesn’t reveal any surprises.
In this setup, the pack aligns against a clamp on the left side and to a parallel block (removed while cutting) along the rear edge of the tooling plate. I could then unclamp the pack, rotate it to put the next edge in place, and use the same XYZ origin with the edge parallel to X.
Here’s the view from the back of the table.
Sawing the case
I ran the spindle at 5 k RPM and cut about 15 inch/secminute. I’m sure the pros do it faster, but that was enough to warm up the blade and that’s fast enough for me. [Update: typo on the units. Thanks!]
Cuts were 0.020 inch per pass, which is about 0.5 mm. I expected the case to be some hard-metric dimension and wasn’t disappointed.
After the cuts reached 0.060 inch, I manage to pry the remaining plastic in the joint apart and split the halves apart along the connectors and LEDs at the front where I couldn’t do any sawing.
Here’s a close look at the cut, just above the battery terminals. The case turned out to be 2 mm thick, about 0.080 inch, so I was just about all the way through. The cut was perfectly aligned with the case and cracked open neatly along the entire length.
Tight tolerance on the cut depth
An interior view, showing that the cells adhered to the left half of the case and the electronics to the right: of course. I pried the cells loose from the left side, which provided enough access to unsolder the things, as the terminals were against the case. Notice that there’s absolutely nothing between the inside of the case and the outside of the cell, so cutting just slightly too deep would be a Bad Thing™.
First look inside the case
After a bit of work, here’s the entire layout…
Battery pack internal layout
Much to my surprise, the battery consists of two series-connected sets of three cells: 2 x 3.7 V = 7.4 V. I expected three series sets for about 3 x 3.7 = 11.1 V, with a linear regulator down to the 9.0 V output.
As it turns out, they used two switching regulators: the one between the two triplets controls the charging voltage and the one to the lower-left boosts the battery to the pack’s 9.0 V output. I had hoped for a resistor divider that I could tweak to get 9.6 V out, but it certainly wasn’t obvious.
I unsoldered the cells, dismounted the circuit board, and puzzled over it for a bit, after which the problem was obvious.
The story continues tomorrow, with a dramatic denouement…
I have a quartet of nice pin punches with hardened pins in various diameters. I managed to drop the smallest punch, didn’t get my foot under it in time, it struck sparks from the concrete floor when it hit, and the pin snapped.
Not being able to replicate the pin’s neat mushroom head, I contented myself by chopping off a length of music wire and grinding the ends flat. Annealed one end over the kitchen stove, whacked it with another punch to get a flat, and it’s all good.
Replacement pin for punch
The music wire isn’t quite perfectly straight, but you don’t beat on things with a 40-mil punch, anyway.