The Smell of Molten Projects in the Morning

Ed Nisley's Blog: Shop notes, electronics, firmware, machinery, 3D printing, laser cuttery, and curiosities. Contents: 100% human thinking, 0% AI slop.

Category: Machine Shop

Mechanical widgetry

  • Rudy Sunglasses: Back From the Dead

    Clear lens installed
    Clear lens installed

    As expected, the uni-lens on Mary’s Rudy Project sunglasses cracked right up the middle as that stress crack above the nosepiece opened up. The sunglasses came with interchangeable lenses, so I swapped in the clear lens.

    Having used urethane adhesive to mechanically lock the defunct gray lens in place, the broken bits were pretty firmly bonded. I applied a brass hammer and small drift punch to the remaining tabs, pried the debris out of the temples, cleaned the adhesive from the recesses, and snapped the new lens in place. Surprisingly, it popped in and locked securely.

    The nosepiece has never worked satisfactorily: there’s nothing locking the flexible blue-silicone pad to the straight-sided posts that are supposed to hold it. As a result, it tends to pop off at the most inopportune moments.

    Rudy nosepiece
    Rudy nosepiece

    I dotted the posts on one side with cyanoacrylate and the other pair with epoxy to see if either will bond well enough to make a difference. If those fail, I’ll try urethane, although I’m not sure what will happen as the urethane expands in the sockets.

    Anyhow, she now has glasses suitable for biking on cloudy and rainy days… which is much better than a sharp stick (or a bug) in the eye, as we see it.

  • Micropositioner Rehabilitation: Z-axis Slide

    With the planetary reducer off, I could remove all the bits and pieces holding the Z-axis slide to the rest of the positioner.

    Rack drive casing
    Rack drive casing

    Note carefully the three spacing washers near each mounting screw. They hold the slide off the casting body by a very precise amount: they’re each 4 mils thick and prone to vanish in a light breeze. I discovered that each screw had three washers when I flicked one off the workbench and discovered two on the floor.

    The metal plate holding the pinion in place has two flat-head screws to the left and two ramps to the right. The conical points of the two long setscrews on the right bear on the ramps, providing a convenient, if obscure from the outside, way to adjust the slide friction by clamping the pinion shaft. One of the setscrews was partially removed, so a previous owner had evidently tried to reduce the overwhelming stickiness.

    With the washers in a safe place, the pinion cover comes off with only slight encouragement.

    Pinion parts
    Pinion parts

    Plenty of congealed lubricating oil to be found.

    Even without the pinion gear, it was exceedingly difficult to urge the two parts of the slide apart: more congealed oil. Much to my surprise, the slide does not have adjustable gibs: it’s one of those precision-ground gadgets that Just Works. This picture shows all the parts in their gunky glory. Note the random dirt in the rack teeth, along with the goo on the pinion shaft.

    Rack and pinion - disassembled
    Rack and pinion – disassembled

    With everything apart, removing the gunk was a simple matter of toxic solvents and mechanical poking with wood picks and splints

    I filed off the burrs on the shafts, thought briefly about grinding some flats for the setscrews, and decided to leave well enough alone.

    A few dabs of clock oil here & there, reassemble everything in reverse order, and the Z-axis moves gracefully with minimal knob torque. It’s very sensitive to the clamping force of those pointed setscrews, though.

    It’s now easy to discover that the planetary reducer has a 5:1 ratio and the Z-axis moves about 6 mm per turn. Because the reducer uses balls, it slips when the slide jams against something, rather than strip its gears.

    I should clean the other two slides, but a dot of clock oil on each cheered them up enough to let me punt that for a while…

    I like it!

    Micropositioner
    Micropositioner
  • Micropositioner Rehabilitation: Planetary Reducer

    Micropositioner
    Micropositioner

    An old 3-axis micropositioner recently found itself on my electronics workbench, where it should come in handy for SMD soldering, microscopic examination, and similar projects requiring the ability to move something in tiny, precise increments. This picture gives you the general idea; it’s mounted on a magnetic base stuck to a random chunk of sheet steel.

    The knob on the front drives the vertical (Z) axis, with the other two controlling the front-to-back (Y) and left-to-right (X) axes. A rotary joint between the X and Y axes, plus another at the tip of the arm, mean you’re not restricted to orthogonal axes; that may be either a blessing or a curse, depending on what you’re trying to accomplish.

    Unfortunately, the Z axis was essentially immovable: that big knurled knob took a remarkable amount of force to drive the slide. Some Quality Shop Time was in order.

    Planetary reducer - cover
    Planetary reducer – cover

    The thing is a chunk of old-school German engineering: nary a gratuitous plastic part to be seen. The planetary reducer has a cast metal cover secured to the torque arm with an acorn nut, which had obviously been removed several times before, as the cover was somewhat chewed beneath the nut.

    I loosened the two setscrews holding the knob in place, gave it a pull, and … nothing. After a protracted struggle and considerable sub-vocal muttering, the knob came off to reveal a thoroughly scarred shaft. Contrary to what I expected, the shaft did not have flats below the setscrews, so the inevitable screw burrs locked the shaft to the knob.

    Planetary reducer - torque arm
    Planetary reducer – torque arm

    The picture to the left shows the planetary drive and torque arm after I filed off the burrs. Two plastic washers (the top one sits on the spring; it’s not shown here) provide smooth bearing surfaces that hold the knob under firm spring pressure, which prevents the Z axis from descending unless you turn the knob manually.

    Planetary drive output shaft screws
    Planetary drive output shaft screws

    Two more setscrews secure the planetary drive’s output bushing to the Z axis pinion shaft. The picture to the right shows that they’re pretty much inaccessible; one was directly behind a tab holding the drive together, the other was aimed at the shoulder of the casting holding the Z axis slide.

    And, of course, even with the knob in place, I can’t turn the mumble shaft, which is why I’m doing this in the first place. The planetary drive uses balls, rather than gears, and the lubricating oil had long since turned into gummy varnish. I slobbered enough light oil into the drive to loosen the gunk enough to make the drive turn-able, albeit with considerable effort. I urged the input shaft barely enough this-a-way and that-a-way to get access to both of the screws.

    Pinion shaft
    Pinion shaft

    As you’d expect, removing the drive required even more muttering and the application of dangerous tools. The pinion shaft was badly scarred in several places, so this poor thing has been dismantled several times before.

    That was entirely enough for one day. Tomorrow, disassembling the Z-axis slide and cleaning things up…

  • Tchotchke Repair

    Tchotchke epoxy
    Tchotchke epoxy

    Sometimes I get to do an easy one. This dust collector came with the house and sits on the fireplace; one of the little guys fell off when Mary went on a cleaning frenzy. As nearly as I can tell, he had a bad butt weld (using the exact term) with marginal penetration.

    A dot of JB Weld, an uncomfortable overnight stay on the workbench, and he’s as almost good as new. I briefly thought about resistance-soldering him together, but came to my senses: epoxy to the rescue!

    The balance point is sufficiently delicate that the additional weight of the epoxy pulls his side down a bit. I’ll call it art and leave it at that, although I should build a little circuit with a proximity sensor and an electromagnet to keep the thing in motion.

    See-saw tchotche repaired
    See-saw tchotchke repaired

    Yeah, that’s my Tau Beta Pi Bent in the background… along with the little glass bead I made in the Corning Museum of Glass a few summers ago.

  • Bicycle Tire Liner Abrasion

    The front tire (a Primo Comet blackwall) on Mary’s Tour Easy was flat when we rolled out of the garage a few days ago. While a flat isn’t pleasant at any time, it’s much nicer to find one at home, before the ride, rather than out on the road!

    I figured the tire ate something sharp that managed to work its way through the tire liner and into the tube; that’s rare, but it sometimes happens. These two pix of the tread show why we use tire liners: sidewall-to-sidewall nicks, cuts, gouges, and gashes, despite the fact that the herringbone tread has plenty of life left in it. Click the pix to enlarge, if you dare…

    Tire cuts 1
    Tire cuts 1

    And another section; it’s like this all the way around the tire. I think this one is the better part of a year old, so it has maybe 2000 miles on it. It handled 200+ miles along the Pine Creek Gorge rail-trail this past summer, which was sharp crushed gravel, but most of the cuts came from roadside debris on our ordinary utility rides around home.

    Tire cuts 2
    Tire cuts 2

    As it turned out, the tire liner had prevented all those punctures from reaching the tube, while killing the tube all by itself. The sharp edge where the the two ends of the liner overlap had worried its way through the tube.

    Abrasion from tire liner
    Abrasion from tire liner

    The tire liner wasn’t a genuine fluorescent green Slime strip, but some translucent brown thing. The difference: Slime liners are thinner and don’t have nearly this much abrasive power.

    Alas, I didn’t have a Slime liner in my stash (remedied with the most recent bike parts order), so I put the brown liner back in with a few layers of genuine Scotch electrical tape to build the end up a bit. There’s really no good way to feather the end without making it into a ragged knife edge.

    New tire and tube, of course. I’m not that crazy!

    With any luck, the liner and tape will behave for another few years, until the tire wears out, and then I’ll replace everything. Other than this event, flats aren’t a big part of our riding experience.

  • Whirlpool Refrigerator Shelf: Drawer Slide Repair

    Refrigerator shelf bracket - inside
    Refrigerator shelf bracket – inside

    The bottom glass shelf in our Whirlpool refrigerator (the “Crisper Cover”) rests on an elaborate plastic structure that includes slides for the two Crisper drawers. Perhaps we store far more veggies than they anticipated, we’re rough on our toys, or the drawer slides came out a whole lot weaker than the designers expected. I’m betting on the latter, but whatever the cause, the two outside slides broke some years ago.

    I don’t know what function the rectangular hole above the flattened part of the slide might serve, but it acted as a stress raiser that fractured the column toward the front. With that end broken loose, another crack propagated toward the rear, so the entire front end of the slide drooped when the drawer slid forward.

    The minimum FRU (Field Replacement Unit) is the entire plastic shelf assembly, a giant plastic thing that fills the entire bottom of the refrigerator. You could, of course, buy a whole new shelf assembly, perhaps from www.appliancepartspros.com, but it’s no longer available. Back when it was, I recall it being something on the far side of $100, which made what you see here look downright attractive.

    My first attempt at a repair was an aluminum bracket epoxied to the outside of the slide, filling the rectangular opening with JB Industro-Weld epoxy to encourage things to stay put. The plastic cannot be solvent-bonded with anything in my armory, so I depended on epoxy’s griptivity to lock the aluminum into the shelf. That worked for maybe five years for the right side (shown above) and is still working fine on the left side.

    Refrigerator shelf bracket - bottom
    Refrigerator shelf bracket – bottom

    The right-side bracket eventually broke loose, so I did what I should have done in the first place: screw the bracket to the shelf. Alas, my original bracket remained firmly bonded to the bottom part of the shelf and secured to the block of epoxy in the rectangular hole. Remember, the broken piece didn’t completely separate from the shelf.

    So I cut another angle bracket to fit around the first, drilled holes in the shelf, transfer-punched the bracket, and match-drilled the holes. Some short(ened) stainless-steel screws and nuts held the new bracket in place and a few dabs of epoxy putty filled the gaps to make everything rigid.

    That’s been working for the last few years. The refrigerator is going on 16 years with only one major repair (a jammed-open defrost switch), so I’ll call it good enough.

  • Improvised Snowthrower Skid Shoes

    Our snowthrower rests the entire weight of the front end on a pair of skid shoes, which erode against the asphalt driveway. Replacements cost nigh onto eleven bucks each, which activates my cheapskate gene.

    Worn OEM skid shoes
    Worn OEM skid shoes

    You can see from the markings that the slots are about twice as long as they need to be, so I figured I could replace them with some random angle iron. Might not last as long, but far less expensive.

    Bedframe skid shoe
    Bedframe skid shoe

    Having a nearly infinite supply of bedframe steel in the heap, I chopped off two suitable lengths, poked 3/8″ holes into the appropriate spots, then milled short slots to get some adjustability.

    Bedframe steel is about the nastiest stuff you (well, I) can still machine: high carbon, fine blue-hot chips, and hard edges. It might actually be better-suited for skid shoes than the soft steel OEM parts.

    They’re not pretty, but the driveway hasn’t complained yet.

    The only real problem is that those sharp corners snag on the edges of what we loosely term “the lawn”. I should apply the smoke wrench, miter the corners, and bend the edges upward. If I’m going to all that trouble, I should also hitch up the buzz box and wave some hardfacing ‘trodes over the bottom.

    But that’s in the nature of fine tuning and sounds a lot like work.