These mailings generally carry a “trash before reading” interest level, but this one stands out:
The Terms and Conditions feature some gems:
The first few sections suggest their past behavior has required some … admissions … to avoid future issues.
Section 9 says the laws of Florida apply and the “agreement is performable” (whatever that means) “at United Directories’ address located in Jacksonville Beach, Florida”. They’re so afraid of their customers that the only address appearing on the mailer is in Atlanta, Georgia, but a bit of poking around suggests their HQ is inside what looks like a beachfront house across from Joe’s Crab Shack or a biz building up the street.
Section 11 says your “listing” will be renewed every six months at $396, so you pay nigh onto 800 bucks a year for a “customizable web page” nobody visits.
Section 12 tells you “Unpaid accounts will incur a 10% late charge” and “Any credits will be applied to the next subscription period.”
I wired a resistive joystick to the knockoff Nano controlling the crystal tester and connected the button to an analog input because I have a lot of those left over and why not. Unfortunately, the ADC returned a sequence of random-ish numbers indicating the button didn’t have a pullup to +5 V.
One might be forgiven for assuming the pads marked R5 would hold such a pullup resistor, had the joystick not been relentlessly cost-reduced:
One would, of course, be completely wrong.
Having been around this blockseveral times, I measured the pad-to-pin resistances and found R5 firmly affixed to the GND and +5V pins, with the SW (a.k.a. button) pin floating free. Pressing the joystick hat closes the switch next to R5, thereby connecting the SW pin to GND.
Baffles me. Maybe a fresh intern did the PCB layout and just misplaced the resistor?
So I soldered an ordinary resistor (*) between the +5 V and SW pins:
Now it works just as it should.
(*) For long-lost reasons, I have a zillion 12.4 kΩ 1% resistors appearing in place of simple 10 kΩ resistors.
The plotter I received works beautifully, except that the carousel doesn’t rotate. I found a YouTube video showing a 7475a running with the cover off, and there’s a little plastic piece – it looks like a teardrop – that advances the carousel, and is apparently part of the carousel motor assembly. Mine is missing that piece …
The keyword is Geneva drive, a wonderfully simple technique to convert one rotation of the stepper motor into 1/6 turn of the pen carousel, with no need for fancy sensors.
Back in the day, you could get the entire Pen Carousel Housing Assembly w/ Motor (PN 07475-60175) as a unit and the Carousel Motor Only(PN 3140-0687) as a separate thing, but not the Geneva drive wheel:
The cam’s drive wheel end (in inches, because early 1980s):
0.25 thick overall
0.10 thick plate under pin end
1.09 OD – rounded end
The pin sticking up from the cam:
0.154 OD (or fit to slot?)
0.16 tall (above base plate)
I have no good (i.e., easy + accurate) way to measure the distance from the motor shaft to the pin, but I doubt it’s critical. As long as the pin doesn’t quite whack the hub end of the slot, it’s all good:
The 0.10 plate + 0.16 pin height don’t quite add up to the 0.25 overall measurement, but that’s certainly measurement error. I’d round the pin length downward and carve the drive from a 1/4 inch sheet.
A 3D printed part would probably work, apart from the accuracy required to fit the D-shaped motor shaft. Perhaps a round hole, reamed to fit the shaft, carefully aligned / positioned, with epoxy filling the D-shaped void, would suffice. A dent in the round hole would give the epoxy something to grab.
I’d be sorely tempted to use an actual metal / plastic rod for the pin, rather than depend on a stack of semi-fused plastic disks. The pin must withstand hitting the end of the “missing” slot during the power-on indexing rotation, because turning the carousel isn’t quite a non-contact sport. Normally, though, it enters the end of the slot without much fuss:
The blocked slot sits at the bottom of that picture, with a small locating pin sticking upward just above the circular feature at the end of the arm: we’re seeing the negative of a plug inserted into the original injection mold.
The SOIC chip pattern sits at right angles to the DIP pins, which took some getting used to.
The slightly defocused wire connecting pin 4 (on the IC) to pins 5, 6, and 7 (on the PCB) selects address 0x48.
So I flipped it over, soldered four wires (+5 V, GND, SDA, SCL) to the numbered pins on bottom of the board, made up a little header for the other end, wired a socket strip on the crystal tester board, plugged it in, and … nothing worked.
Turns out that the other side of the board carries a TSSOP pattern, which I’d neatly masked off with a snippet of Kapton tape, surrounded by eight numbered pins. Of course, those pin numbers correspond to the TSSOP pattern facing you, so they’re mirror-imaged for the SOIC pattern on the other side.
Soooo, the proper wiring for the SOIC pattern as seen from the TSSOP side has the pin numbers exactly bass-ackwards:
The insulation looked a lot better the first time I soldered the wires to the PCB. Honest.
Anyhow, when correctly wired, the LM75A worked as it should:
It’s snuggled chip-down against the top of the 125 MHz oscillator can, with a dab of heatsink compound improving their thermal bond and a yellow cable tie around the foam holding them together. The socket header is wired pin-for-pin to the DAC I²C socket directly above it.
The OLED temperature display shows 28.250 °C, because the oscillator just started up in a cool basement. It’ll eventually settle around 39-ish °C, where its output should be pretty close to the 125 MHz – 344 Hz value hardcoded into the source.
Oh, that’s a 3 mm amber LED next to the relay can: much less glaring than the white LED, no matter what it looks like here.
The mailing tube arrived with contents intact, although the USPS inlet scanning didn’t work and the tube pretty much teleported across several states without leaving any tracking data behind. The recipient suggested several modifications to the caps:
Review of user experience of tube end:
The ribs on the endcap are very good at holding the cap on, so much so that I had to use a prying implement to remove it, which cracked the flange.
Would consider less depth on the cap, and possibly another layer on the flange.
Some continuous process improvement (a.k.a OpenSCAD hackage) produced a swoopy threaded cap with thumb-and-finger grips:
The finger grips are what’s left after stepping a sphere out of the cap while rotating it around the middle:
That worked out surprisingly well, with the deep end providing enough of a vertical-ish surface to push against.
The two hex holes fit a pin wrench, because the grips twist only one way: outward. The wrench eliminates the need for a flange, as you can now adjust the cap insertion before slathering packing tape over the ends. Man, I loves me some good late binding action!
A three-start thread seemed like overkill, but was quick & easy. The “thread form” consists of square rods sunk into the cap perimeter, with one edge sticking out:
They’re 1.05 times longer than the cap perimeter facets to make their ends overlap, although they’re not tapered like the ones in the broom handle dingus, because it didn’t (seem to) make any difference to the model’s manifoldhood.
Not needing any endcaps right now, I built one for show-n-tell:
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